Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2013-06-06 — TX
Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2013-06-06 09:15
Report number
Location
TX
Narrative
A leak was observed under the 20" over pressure relief line valve for tank 3802. A loose bleeder valve was determined to be the cause of the leak. The valve was tightened to mitigae the leak. Soil remediation was completed and valve reurned to service.
Detailed record list
Report Received Date
2013-06-25 00:00:00
Iyear
2013
Report Number
20130224
Supplemental Number
18280
Report Type
Supplemental Final
Operator Id
30829
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-06-06 09:15:00
Location Latitude
28.920722
Location Longitude
-98.141111
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.71
Recovered Bbls
0.71
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lyssy Station
Onshore State Abbreviation
Tx
Onshore Postal Code
78113
Onshore City Name
Falls City, Texas
Onshore County Name
Wilson
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Pipe Facility Type
Intrastate
Item Involved
Relief Line And Relief Equipment
Release Type
Leak
Leak Type
Connection Failure
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
70
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
3000
Est Cost Other
0
Prpty
3070
Pipeline Function
< 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Preparer Name
S**** D****
Preparer Title
Senior Pipeline Compliance Engineer
Preparer Email
S******@e****.com
Preparer Telephone
713-381-6487
Prepared Date
2013-07-09 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713-381-6487
Authorizer Title
Senior Pipeline Compliance Engineer
Authorizer Email
S******@e****.com
Narrative
A leak was observed under the 20" over pressure relief line valve for tank 3802. A loose bleeder valve was determined to be the cause of the leak. The valve was tightened to mitigae the leak. Soil remediation was completed and valve reurned to service.
| Report Received Date | 2013-06-25 00:00:00 |
|---|---|
| Iyear | 2013 |
| Report Number | 20130224 |
| Supplemental Number | 18280 |
| Report Type | Supplemental Final |
| Operator Id | 30829 PHMSA Enforcement |
| Name | Enterprise Crude Pipeline Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2013-06-06 09:15:00 |
| Location Latitude | 28.920722 Google Maps OpenStreetMap |
| Location Longitude | -98.141111 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.71 |
| Recovered Bbls | 0.71 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Lyssy Station |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 78113 |
| Onshore City Name | Falls City, Texas |
| Onshore County Name | Wilson |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Tank, Including Attached Appurtenances |
| Pipe Facility Type | Intrastate |
| Item Involved | Relief Line And Relief Equipment |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 70 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 3000 |
| Est Cost Other | 0 |
| Prpty | 3070 |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Defective Or Loose Tubing Or Fitting |
| Eq Failure Type | Defective Or Loose Tubing Or Fitting |
| Preparer Name | S**** D**** |
| Preparer Title | Senior Pipeline Compliance Engineer |
| Preparer Email | S******@e****.com |
| Preparer Telephone | 713-381-6487 |
| Prepared Date | 2013-07-09 00:00:00 |
| Authorizer Name | S**** D**** |
| Authorizer Telephone | 713-381-6487 |
| Authorizer Title | Senior Pipeline Compliance Engineer |
| Authorizer Email | S******@e****.com |
| Narrative | A leak was observed under the 20" over pressure relief line valve for tank 3802. A loose bleeder valve was determined to be the cause of the leak. The valve was tightened to mitigae the leak. Soil remediation was completed and valve reurned to service. |
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