HL incident on 2013-05-23 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,000
Incident datetime
2013-05-23 18:39
Report number
Location
OK
Narrative
During an investigative dig following an in-line inspection, a petroleum odor was found as soil was excavated. Additional searching reveal a crack in the pipe, resulting in the release. The pipe was replaced with new, pre-tested pipe and the impacted soil was remediated in accordance with company and state standards.
Detailed record list
Report Received Date
2013-06-22 00:00:00
Iyear
2013
Report Number
20130223
Supplemental Number
18997
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2013-05-23 18:39:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.12
Recovered Bbls
0.12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Down For Rehab Following An In-Line Inspection.
Nrc Rpt Datetime
2013-05-23 10:22:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Remotely Controlled
Pipe Fac Name
Alexandria To Fargo #2-8" Line
Segment Name
Line Id #6270
Onshore State Abbreviation
Mn
Onshore Postal Code
56514
Onshore City Name
Barnesville
Onshore County Name
Wilkin
Designated Location
Milepost/valve Station
Designated Name
77
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
28
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
8.625
Pipe Wall Thickness
0.203
Pipe Smys
42000
Pipe Specification
Api-5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Kaiser Steel
Pipe Coating Type
Coal Tar
Installation Year
1954
Manufactured Year
1954
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
0.12
Rel Water Name
Shallow Groundwater Table
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
800
Est Cost Gas Released
35
Est Cost Prop Damage
3000
Est Cost Emergency
23000
Est Cost Environmental
10000
Est Cost Other
0
Prpty
36835
Accident Psig
300
Mop Psig
1186
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
201462
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release feature was found during rehabilitation of the line following an in-line inspection. Given that the release was from an anomaly in the pipe, there is no evidence linking the control room to the release. Neither is there evidence that the controller on duty caused or contributed to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Fatigue Vibr Related
Yes
Failure Subtype
Pressure-Related
Additional Crack Ind
Yes
Collected Data Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Circ Wave Recent Year
2012
Geometry Recent Year
2012
Other Recent Year
2007
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1989
Hydrtst Most Rcnt Pressure
1858
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7377
Prepared Date
2014-02-07 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
During an investigative dig following an in-line inspection, a petroleum odor was found as soil was excavated. Additional searching reveal a crack in the pipe, resulting in the release. The pipe was replaced with new, pre-tested pipe and the impacted soil was remediated in accordance with company and state standards.
Report Received Date 2013-06-22 00:00:00
Iyear 2013
Report Number 20130223
Supplemental Number 18997
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2013-05-23 18:39:00
Location Latitude 46.6178 Google Maps OpenStreetMap
Location Longitude -96.4543 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.12
Recovered Bbls 0.12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Down For Rehab Following An In-Line Inspection.
Nrc Rpt Datetime 2013-05-23 10:22:00
Nrc Rpt Num 1048175 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Remotely Controlled
Pipe Fac Name Alexandria To Fargo #2-8" Line
Segment Name Line Id #6270
Onshore State Abbreviation Mn
Onshore Postal Code 56514
Onshore City Name Barnesville
Onshore County Name Wilkin
Designated Location Milepost/valve Station
Designated Name 77
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 28
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 8.625
Pipe Wall Thickness 0.203
Pipe Smys 42000
Pipe Specification Api-5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Kaiser Steel
Pipe Coating Type Coal Tar
Installation Year 1954
Manufactured Year 1954
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 0.12
Rel Water Name Shallow Groundwater Table
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 800
Est Cost Gas Released 35
Est Cost Prop Damage 3000
Est Cost Emergency 23000
Est Cost Environmental 10000
Est Cost Other 0
Prpty 36835
Accident Psig 300
Mop Psig 1186
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 201462
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release feature was found during rehabilitation of the line following an in-line inspection. Given that the release was from an anomaly in the pipe, there is no evidence linking the control room to the release. Neither is there evidence that the controller on duty caused or contributed to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Fatigue Vibr Related Yes
Failure Subtype Pressure-Related
Additional Crack Ind Yes
Collected Data Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Circ Wave Recent Year 2012
Geometry Recent Year 2012
Other Recent Year 2007
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1989
Hydrtst Most Rcnt Pressure 1858
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name K****** L* L*******
Preparer Title Sr. Compliance Coordinator
Preparer Email K***********@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7377
Prepared Date 2014-02-07 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Sr. Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative During an investigative dig following an in-line inspection, a petroleum odor was found as soil was excavated. Additional searching reveal a crack in the pipe, resulting in the release. The pipe was replaced with new, pre-tested pipe and the impacted soil was remediated in accordance with company and state standards.

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