Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2013-05-22 — TX
Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$5,000
Incident datetime
2013-05-22 14:15
Report number
Location
TX
Narrative
An oil leak was observed by air patrol and when investigated by station technician it was discovered that a valve was leaking because of loose bolts. Bolts were tightened and leak stopped.
Detailed record list
Report Received Date
2013-06-20 00:00:00
Iyear
2013
Report Number
20130218
Supplemental Number
18533
Report Type
Supplemental Final
Operator Id
30829
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-05-22 14:15:00
Location Latitude
34.092292
Location Longitude
-98.90449
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-05-22 14:15:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-05-22 14:15:00
Restart Datetime
2013-05-22 16:30:00
On Site Datetime
2013-05-22 15:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Electra Station
Onshore State Abbreviation
Tx
Onshore Postal Code
76360
Onshore County Name
Wichita
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Release Type
Leak
Leak Type
Connection Failure
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
250
Est Cost Prop Damage
5000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
5250
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Preparer Name
S**** D****
Preparer Title
Senior Pipeline Compliance Engineer
Preparer Email
S******@e****.com
Preparer Telephone
713-381-6487
Prepared Date
2013-09-10 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713-381-6487
Authorizer Title
Senior Pipeline Compliance Engineer
Authorizer Email
S******@e****.com
Narrative
An oil leak was observed by air patrol and when investigated by station technician it was discovered that a valve was leaking because of loose bolts. Bolts were tightened and leak stopped.
| Report Received Date | 2013-06-20 00:00:00 |
|---|---|
| Iyear | 2013 |
| Report Number | 20130218 |
| Supplemental Number | 18533 |
| Report Type | Supplemental Final |
| Operator Id | 30829 PHMSA Enforcement |
| Name | Enterprise Crude Pipeline Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2013-05-22 14:15:00 |
| Location Latitude | 34.092292 Google Maps OpenStreetMap |
| Location Longitude | -98.90449 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 1 |
| Recovered Bbls | 1 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2013-05-22 14:15:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2013-05-22 14:15:00 |
| Restart Datetime | 2013-05-22 16:30:00 |
| On Site Datetime | 2013-05-22 15:00:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Electra Station |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 76360 |
| Onshore County Name | Wichita |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Valve |
| Valve Type | Auxiliary Or Other Valve |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 250 |
| Est Cost Prop Damage | 5000 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 5250 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Other Equipment Failure |
| Eq Failure Type | Other Equipment Failure |
| Preparer Name | S**** D**** |
| Preparer Title | Senior Pipeline Compliance Engineer |
| Preparer Email | S******@e****.com |
| Preparer Telephone | 713-381-6487 |
| Prepared Date | 2013-09-10 00:00:00 |
| Authorizer Name | S**** D**** |
| Authorizer Telephone | 713-381-6487 |
| Authorizer Title | Senior Pipeline Compliance Engineer |
| Authorizer Email | S******@e****.com |
| Narrative | An oil leak was observed by air patrol and when investigated by station technician it was discovered that a valve was leaking because of loose bolts. Bolts were tightened and leak stopped. |
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