Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2013-04-24 — OH
Operator
Marathon Pipe Line Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$195,329
Incident datetime
2013-04-24 20:00
Report number
Location
OH
Narrative
6/20/2013 - a leak was identified on the discharge side of mainline pump within elwood station. The gasket has been repaired. The gasket was sent for failure analysis. Update: note that in part a, question 18a - the pipeline was shutdown at 12:55 but this reporting system would not allow the shutdown time to be before the identified leak time of 20:00. This leak was in a historical site and the pipeline was shutdown as a precaution. This supplemental reflects updated costs. Update 11/19/2013: updated final costs update 1/16/2014: the gasket was sent out for metallurgical analysis to garlock. The report stated that the gasket had become unwound for an unknown reason.
Detailed record list
Report Received Date
2013-06-20 00:00:00
Iyear
2013
Report Number
20130217
Supplemental Number
18926
Report Type
Supplemental Final
Operator Id
32147
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2013-04-24 20:00:00
Location Latitude
40.291729
Location Longitude
-85.862736
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.2
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2013-04-24 20:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-04-24 20:00:00
Restart Datetime
2013-04-26 02:00:00
On Site Datetime
2013-04-24 20:00:00
Nrc Rpt Datetime
2013-04-24 23:00:00
Nrc Rpt Num
1045017
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Martinsville - Lima 22"
Segment Name
Elwood - Bryant 22"
Onshore State Abbreviation
In
Onshore Postal Code
46036
Onshore City Name
Elwood
Onshore County Name
Tipton
Designated Location
Survey Station No.
Designated Name
6810+04
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Garlock Gasket
Installation Year
1993
Material Involved
Material Other Than Carbon Steel
Material Details
Flex Graphite, 304 Stainless Winding
Release Type
Leak
Leak Type
Connection Failure
Leak Type Other
Gasket
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
40
Est Cost Prop Damage
195329
Est Cost Emergency
17180
Est Cost Environmental
0
Est Cost Other
0
Prpty
212549
Accident Psig
980
Mop Psig
1431
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Eq Additional Other Ind
Yes
Eq Additional Other Details
Spiral Wound Gasket Came Unwound
Preparer Name
R**** S********
Preparer Title
Hes Regulatory Compliance
Preparer Email
R**********@m****************.com
Preparer Telephone
419-421-2121
Prepared Date
2014-01-16 00:00:00
Authorizer Name
R****** B*****
Authorizer Telephone
419-421-2121
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
6/20/2013 - a leak was identified on the discharge side of mainline pump within elwood station. The gasket has been repaired. The gasket was sent for failure analysis. Update: note that in part a, question 18a - the pipeline was shutdown at 12:55 but this reporting system would not allow the shutdown time to be before the identified leak time of 20:00. This leak was in a historical site and the pipeline was shutdown as a precaution. This supplemental reflects updated costs. Update 11/19/2013: updated final costs update 1/16/2014: the gasket was sent out for metallurgical analysis to garlock. The report stated that the gasket had become unwound for an unknown reason.
| Report Received Date | 2013-06-20 00:00:00 |
|---|---|
| Iyear | 2013 |
| Report Number | 20130217 |
| Supplemental Number | 18926 |
| Report Type | Supplemental Final |
| Operator Id | 32147 PHMSA Enforcement |
| Name | Marathon Pipe Line Llc |
| Operator Street Address | 539 South Main Street |
| Operator City Name | Findlay |
| Operator State Abbreviation | OH |
| Operator Postal Code | 45840 |
| Local Datetime | 2013-04-24 20:00:00 |
| Location Latitude | 40.291729 Google Maps OpenStreetMap |
| Location Longitude | -85.862736 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.2 |
| Recovered Bbls | 0.2 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2013-04-24 20:00:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2013-04-24 20:00:00 |
| Restart Datetime | 2013-04-26 02:00:00 |
| On Site Datetime | 2013-04-24 20:00:00 |
| Nrc Rpt Datetime | 2013-04-24 23:00:00 |
| Nrc Rpt Num | 1045017 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Martinsville - Lima 22" |
| Segment Name | Elwood - Bryant 22" |
| Onshore State Abbreviation | In |
| Onshore Postal Code | 46036 |
| Onshore City Name | Elwood |
| Onshore County Name | Tipton |
| Designated Location | Survey Station No. |
| Designated Name | 6810+04 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Other |
| Item Involved Details | Garlock Gasket |
| Installation Year | 1993 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Flex Graphite, 304 Stainless Winding |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Leak Type Other | Gasket |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| Other Pop Ind | Yes |
| Other Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 40 |
| Est Cost Prop Damage | 195329 |
| Est Cost Emergency | 17180 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 212549 |
| Accident Psig | 980 |
| Mop Psig | 1431 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | Yes, specify investigation result(s): (select all that apply) |
| Invest Schedule Ind | Yes |
| Invest No Control Room Ind | Yes |
| Invest No Controller Ind | Yes |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | Gasket |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Spiral Wound Gasket Came Unwound |
| Preparer Name | R**** S******** |
| Preparer Title | Hes Regulatory Compliance |
| Preparer Email | R**********@m****************.com |
| Preparer Telephone | 419-421-2121 |
| Prepared Date | 2014-01-16 00:00:00 |
| Authorizer Name | R****** B***** |
| Authorizer Telephone | 419-421-2121 |
| Authorizer Title | Regulatory Compliance Supervisor |
| Authorizer Email | R*******@m****************.com |
| Narrative | 6/20/2013 - a leak was identified on the discharge side of mainline pump within elwood station. The gasket has been repaired. The gasket was sent for failure analysis. Update: note that in part a, question 18a - the pipeline was shutdown at 12:55 but this reporting system would not allow the shutdown time to be before the identified leak time of 20:00. This leak was in a historical site and the pipeline was shutdown as a precaution. This supplemental reflects updated costs. Update 11/19/2013: updated final costs update 1/16/2014: the gasket was sent out for metallurgical analysis to garlock. The report stated that the gasket had become unwound for an unknown reason. |
External Resources
PHMSA pipeline safety insights.
Product
Features
Company
All rights reserved. Copyright © by ClearPHMSA