HL incident on 2013-05-20 — TX

Operator
Sunoco Pipeline L.p.
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2013-05-20 09:45
Report number
Location
TX
Narrative
A 12 inch strainer lid closure o-ring failed and leaked gasoline at the twin oaks pump station. The strainer leak was discovered by an employee. Gasoline was observed dripping from a 12 inch strainer configured with a meter run on the 8" twin-iced pipeline. The pipeline was shut down. Immediate measures were taken to control and contain the leak. Company personnel and contract osro emergency responders were organized to address the clean-up effort following incident command structure. An nrc report # 1047704 was made because sheen on water was discovered. Upon opening the strainer, it was determined that the strainer closure o-ring had failed. Immediate cause of the o-ring failure was seam separation.
Detailed record list
Report Received Date
2013-06-19 00:00:00
Iyear
2013
Report Number
20130214
Supplemental Number
18844
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-05-20 09:45:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
5.3
Recovered Bbls
5.3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2013-05-20 09:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-05-20 09:48:00
Restart Datetime
2013-05-20 19:53:00
On Site Datetime
2013-05-20 09:45:00
Nrc Rpt Datetime
2013-05-20 11:10:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Twin Oaks Pump Station
Segment Name
Twin-Iced 8
Onshore State Abbreviation
Pa
Onshore Postal Code
19013
Onshore City Name
Upper Chichester
Onshore County Name
Delaware
Designated Location
Milepost/valve Station
Designated Name
0 + 00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Strainer In Meter Run On Suction Of Pump
Installation Year
1968
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
Yes
Fish Aquatic Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
0.5
Rel Water Name
Un-Named Tributary To Harveys Run
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
672
Est Cost Prop Damage
0
Est Cost Emergency
35000
Est Cost Environmental
10000
Est Cost Other
0
Prpty
45672
Accident Psig
40
Mop Psig
740
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak was a drip that was not detectable by control room operators using cpm or scada controls.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
O-Ring Separation At Seam.
Preparer Name
A* K******
Preparer Title
Dot Compliance Specialist
Preparer Email
A********@s**************.com
Preparer Telephone
610-859-5755
Preparer Fax
800-741-1888
Prepared Date
2013-12-18 00:00:00
Authorizer Name
A* K******
Authorizer Telephone
610-859-5755
Authorizer Title
Dot Compliance Specialist
Authorizer Email
A********@s**************.com
Narrative
A 12 inch strainer lid closure o-ring failed and leaked gasoline at the twin oaks pump station. The strainer leak was discovered by an employee. Gasoline was observed dripping from a 12 inch strainer configured with a meter run on the 8" twin-iced pipeline. The pipeline was shut down. Immediate measures were taken to control and contain the leak. Company personnel and contract osro emergency responders were organized to address the clean-up effort following incident command structure. An nrc report # 1047704 was made because sheen on water was discovered. Upon opening the strainer, it was determined that the strainer closure o-ring had failed. Immediate cause of the o-ring failure was seam separation.
Report Received Date 2013-06-19 00:00:00
Iyear 2013
Report Number 20130214
Supplemental Number 18844
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-05-20 09:45:00
Location Latitude 39.8411 Google Maps OpenStreetMap
Location Longitude -75.4177 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 5.3
Recovered Bbls 5.3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2013-05-20 09:45:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-05-20 09:48:00
Restart Datetime 2013-05-20 19:53:00
On Site Datetime 2013-05-20 09:45:00
Nrc Rpt Datetime 2013-05-20 11:10:00
Nrc Rpt Num 1047704 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Twin Oaks Pump Station
Segment Name Twin-Iced 8
Onshore State Abbreviation Pa
Onshore Postal Code 19013
Onshore City Name Upper Chichester
Onshore County Name Delaware
Designated Location Milepost/valve Station
Designated Name 0 + 00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Strainer In Meter Run On Suction Of Pump
Installation Year 1968
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind Yes
Fish Aquatic Impact Ind Yes
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 0.5
Rel Water Name Un-Named Tributary To Harveys Run
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 672
Est Cost Prop Damage 0
Est Cost Emergency 35000
Est Cost Environmental 10000
Est Cost Other 0
Prpty 45672
Accident Psig 40
Mop Psig 740
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak was a drip that was not detectable by control room operators using cpm or scada controls.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details O-Ring Separation At Seam.
Preparer Name A* K******
Preparer Title Dot Compliance Specialist
Preparer Email A********@s**************.com
Preparer Telephone 610-859-5755
Preparer Fax 800-741-1888
Prepared Date 2013-12-18 00:00:00
Authorizer Name A* K******
Authorizer Telephone 610-859-5755
Authorizer Title Dot Compliance Specialist
Authorizer Email A********@s**************.com
Narrative A 12 inch strainer lid closure o-ring failed and leaked gasoline at the twin oaks pump station. The strainer leak was discovered by an employee. Gasoline was observed dripping from a 12 inch strainer configured with a meter run on the 8" twin-iced pipeline. The pipeline was shut down. Immediate measures were taken to control and contain the leak. Company personnel and contract osro emergency responders were organized to address the clean-up effort following incident command structure. An nrc report # 1047704 was made because sheen on water was discovered. Upon opening the strainer, it was determined that the strainer closure o-ring had failed. Immediate cause of the o-ring failure was seam separation.

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