HL incident on 2013-05-10 — OH

Operator
Marathon Pipe Line Llc
Cause
Other Outside Force Damage
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$384,650
Incident datetime
2013-05-10 04:45
Report number
Location
OH
Narrative
An estimated release of 539 barrels of diesel fuel was discovered on may 9, 2013. The release was caused by a third party's copper wire laid over the pipeline that caused an electrical arc.
Detailed record list
Report Received Date
2013-06-06 00:00:00
Iyear
2013
Report Number
20130198
Supplemental Number
19502
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2013-05-09 04:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
539
Recovered Bbls
539
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2013-05-10 04:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Down Per Schedule.
On Site Datetime
2013-05-10 04:45:00
Nrc Rpt Datetime
2013-05-09 09:26:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Speedway Rio 8"
Segment Name
Speedway Rio 8"
Onshore State Abbreviation
In
Onshore Postal Code
46254
Onshore City Name
Indianapolis
Onshore County Name
Marion
Designated Location
Milepost/valve Station
Designated Name
250+35
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
96
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.32
Pipe Smys
35000
Pipe Specification
Api-5l-Grade B
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1950
Manufactured Year
1950
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Electrical Surge Burn Through
Wildlife Impact Ind
Yes
Fish Aquatic Impact Ind
Yes
Birds Impact Ind
Yes
Terrestrial Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Wildlife Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
490
Rel Water Name
A Drainage Ditch And Retention Pond
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
27000
Est Cost Prop Damage
384650
Est Cost Emergency
3636400
Est Cost Environmental
1880000
Est Cost Other
0
Prpty
5928050
Accident Psig
221
Mop Psig
1496
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
Yes
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest Other Ind
Yes
Invest Other Ind Details
Neither A Controller Nor A Control Room Issue Was The Cause Of Or A Contributing Factor To The Accident. However, Occurrence Of The Accident Possibly Could Have Been Identified Sooner Through Further Investigation Of And Action On Slack Line Alarms Received On 4/24/13.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Electrical Arcing From Other Equipment Or Facility
Outside Force Type
Electrical Arcing From Other Equipment Or Facility
Preparer Name
R**** S********
Preparer Title
Hes Professional
Preparer Email
R**********@m****************.com
Preparer Telephone
419-421-2121
Prepared Date
2014-06-23 00:00:00
Authorizer Name
R****** B*****
Authorizer Telephone
419-421-2121
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
An estimated release of 539 barrels of diesel fuel was discovered on may 9, 2013. The release was caused by a third party's copper wire laid over the pipeline that caused an electrical arc.
Report Received Date 2013-06-06 00:00:00
Iyear 2013
Report Number 20130198
Supplemental Number 19502
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2013-05-09 04:00:00
Location Latitude 39.853611 Google Maps OpenStreetMap
Location Longitude -86.226389 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 539
Recovered Bbls 539
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2013-05-10 04:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Down Per Schedule.
On Site Datetime 2013-05-10 04:45:00
Nrc Rpt Datetime 2013-05-09 09:26:00
Nrc Rpt Num 1046514 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Speedway Rio 8"
Segment Name Speedway Rio 8"
Onshore State Abbreviation In
Onshore Postal Code 46254
Onshore City Name Indianapolis
Onshore County Name Marion
Designated Location Milepost/valve Station
Designated Name 250+35
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 96
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.32
Pipe Smys 35000
Pipe Specification Api-5l-Grade B
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1950
Manufactured Year 1950
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Electrical Surge Burn Through
Wildlife Impact Ind Yes
Fish Aquatic Impact Ind Yes
Birds Impact Ind Yes
Terrestrial Impact Ind Yes
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Wildlife Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 490
Rel Water Name A Drainage Ditch And Retention Pond
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 27000
Est Cost Prop Damage 384650
Est Cost Emergency 3636400
Est Cost Environmental 1880000
Est Cost Other 0
Prpty 5928050
Accident Psig 221
Mop Psig 1496
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind Yes
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest Other Ind Yes
Invest Other Ind Details Neither A Controller Nor A Control Room Issue Was The Cause Of Or A Contributing Factor To The Accident. However, Occurrence Of The Accident Possibly Could Have Been Identified Sooner Through Further Investigation Of And Action On Slack Line Alarms Received On 4/24/13.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Electrical Arcing From Other Equipment Or Facility
Outside Force Type Electrical Arcing From Other Equipment Or Facility
Preparer Name R**** S********
Preparer Title Hes Professional
Preparer Email R**********@m****************.com
Preparer Telephone 419-421-2121
Prepared Date 2014-06-23 00:00:00
Authorizer Name R****** B*****
Authorizer Telephone 419-421-2121
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative An estimated release of 539 barrels of diesel fuel was discovered on may 9, 2013. The release was caused by a third party's copper wire laid over the pipeline that caused an electrical arc.

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