HL incident on 2013-04-30 — TX

Operator
Mobil Pipe Line Company
Cause
Other Outside Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2013-04-30 13:40
Report number
Location
TX
Narrative
Pipeline damage was apparently caused by third party installation of a guy wire to anchor a power pole. The pole was installed in 1984 prior to the missouri one call system. No record found to indicate that any notification was received prior to pole/anchor installation. Ozark borders co-op provided information on the installation date. Incident still under investigation and a supplemental report will be completed upon final investigation. 3-21-14 supplemental report submitted to add missing data in part c, question 3 - added pipe
Detailed record list
Report Received Date
2013-05-30 00:00:00
Iyear
2013
Report Number
20130189
Supplemental Number
19160
Report Type
Supplemental
Operator Id
Name
Mobil Pipe Line Company
Operator Street Address
800 Bell Street Room 623 F
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-04-30 13:40:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.3
Recovered Bbls
1.3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2013-04-30 13:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Previously Shut Down Due To March 29 Release In Mayflower Ar.'
On Site Datetime
2013-04-30 14:10:00
Nrc Rpt Datetime
2013-04-30 15:37:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Pegasus Pipeline System
Segment Name
Doniphan To Strawberry Section
Onshore State Abbreviation
Mo
Onshore Postal Code
63935
Onshore City Name
Doniphan
Onshore County Name
Ripley
Designated Location
Milepost/valve Station
Designated Name
Mp 461.52
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
25
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
20
Pipe Wall Thickness
0.312
Pipe Smys
42000
Pipe Specification
5xl-42
Pipe Seam Type
Seamless
Pipe Manufacturer
National
Pipe Coating Type
Coal Tar
Installation Year
1947
Manufactured Year
1947
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
3
Puncture Circum
0.1
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
5000
Est Cost Gas Released
100
Est Cost Prop Damage
0
Est Cost Emergency
75000
Est Cost Environmental
143000
Est Cost Other
50000
Est Cost Other Details
Repair For Welding , Nde, And Associate Repair Cost.
Prpty
273100
Accident Psig
410
Mop Psig
875
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
328680
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pipeline system was not running and was shut down from a earler incident. The pipeline was being monitored by controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Other Outside Force Damage
Outside Force Type
Other Outside Force Damage
Osf Other Details
Pipeline Damage Was Apparently Caused By Third Party Installation Of A Guy Wire To Anchor A Power Pole. The Pole Was Installed In 1984 Prior To The Missouri One Call System.
Preparer Name
L**** H********
Preparer Title
Pipeline Safety Advisor
Preparer Email
L****************@e*********.com
Preparer Telephone
903-654-5345
Preparer Fax
903-654-5374
Prepared Date
2014-03-21 00:00:00
Authorizer Name
M*** D W******
Authorizer Telephone
713-656-0227
Authorizer Title
Manager- Safety-Health - Environmental
Authorizer Email
M*************@e*********.com
Narrative
Pipeline damage was apparently caused by third party installation of a guy wire to anchor a power pole. The pole was installed in 1984 prior to the missouri one call system. No record found to indicate that any notification was received prior to pole/anchor installation. Ozark borders co-op provided information on the installation date. Incident still under investigation and a supplemental report will be completed upon final investigation. 3-21-14 supplemental report submitted to add missing data in part c, question 3 - added pipe
Report Received Date 2013-05-30 00:00:00
Iyear 2013
Report Number 20130189
Supplemental Number 19160
Report Type Supplemental
Operator Id 12628 PHMSA Enforcement
Name Mobil Pipe Line Company
Operator Street Address 800 Bell Street Room 623 F
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-04-30 13:40:00
Location Latitude 36.57243 Google Maps OpenStreetMap
Location Longitude -90.87867 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.3
Recovered Bbls 1.3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2013-04-30 13:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Previously Shut Down Due To March 29 Release In Mayflower Ar.'
On Site Datetime 2013-04-30 14:10:00
Nrc Rpt Datetime 2013-04-30 15:37:00
Nrc Rpt Num 1045614 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Pegasus Pipeline System
Segment Name Doniphan To Strawberry Section
Onshore State Abbreviation Mo
Onshore Postal Code 63935
Onshore City Name Doniphan
Onshore County Name Ripley
Designated Location Milepost/valve Station
Designated Name Mp 461.52
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 25
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 20
Pipe Wall Thickness 0.312
Pipe Smys 42000
Pipe Specification 5xl-42
Pipe Seam Type Seamless
Pipe Manufacturer National
Pipe Coating Type Coal Tar
Installation Year 1947
Manufactured Year 1947
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 3
Puncture Circum 0.1
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 5000
Est Cost Gas Released 100
Est Cost Prop Damage 0
Est Cost Emergency 75000
Est Cost Environmental 143000
Est Cost Other 50000
Est Cost Other Details Repair For Welding , Nde, And Associate Repair Cost.
Prpty 273100
Accident Psig 410
Mop Psig 875
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 328680
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pipeline system was not running and was shut down from a earler incident. The pipeline was being monitored by controller.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Other Outside Force Damage
Outside Force Type Other Outside Force Damage
Osf Other Details Pipeline Damage Was Apparently Caused By Third Party Installation Of A Guy Wire To Anchor A Power Pole. The Pole Was Installed In 1984 Prior To The Missouri One Call System.
Preparer Name L**** H********
Preparer Title Pipeline Safety Advisor
Preparer Email L****************@e*********.com
Preparer Telephone 903-654-5345
Preparer Fax 903-654-5374
Prepared Date 2014-03-21 00:00:00
Authorizer Name M*** D W******
Authorizer Telephone 713-656-0227
Authorizer Title Manager- Safety-Health - Environmental
Authorizer Email M*************@e*********.com
Narrative Pipeline damage was apparently caused by third party installation of a guy wire to anchor a power pole. The pole was installed in 1984 prior to the missouri one call system. No record found to indicate that any notification was received prior to pole/anchor installation. Ozark borders co-op provided information on the installation date. Incident still under investigation and a supplemental report will be completed upon final investigation. 3-21-14 supplemental report submitted to add missing data in part c, question 3 - added pipe

All rights reserved. Copyright © by ClearPHMSA