HL incident on 2013-04-23 — TX

Operator
Sunoco Pipeline L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50
Incident datetime
2013-04-23 11:30
Report number
Location
TX
Narrative
On 4/23/2013 a release occurred at the corsicana meter setting when a third party electrical contractor removed a flow switch from an active surge relief line. The subsequent investigation revealed that the contractor acted independently and performed unauthorized/unapproved work and in doing so also failed to follow established lo/to procedures. Corrective actions included suspension of the responsible foreman and a reemphasisation on the importance of morning meetings with all contractor and supervisory personnel to review and/or define the daily work plans, review any permitting requirements for the job and the enforcement of group lo/to procedures.
Detailed record list
Report Received Date
2013-05-21 00:00:00
Iyear
2013
Report Number
20130174
Supplemental Number
18801
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-04-23 11:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-04-23 11:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
System Was Not Operating At The Time.
On Site Datetime
2013-04-23 11:35:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Corsicana Tank Farm
Segment Name
Ringgold 16" Inbound Meter Setting
Onshore State Abbreviation
Tx
Onshore Postal Code
75110
Onshore City Name
Corsicana
Onshore County Name
Navarro
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Relief Line And Relief Equipment
Release Type
Other
Release Type Details
A Third Party Electrical Contractor Removed A Flow Switch From An Active Surge Relief Line.
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
343
Est Cost Prop Damage
50
Est Cost Emergency
500
Est Cost Environmental
23122
Est Cost Other
0
Prpty
24015
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Specialist
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
281-637-6425
Prepared Date
2013-12-06 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Specialist
Authorizer Email
T*********@s**************.com
Narrative
On 4/23/2013 a release occurred at the corsicana meter setting when a third party electrical contractor removed a flow switch from an active surge relief line. The subsequent investigation revealed that the contractor acted independently and performed unauthorized/unapproved work and in doing so also failed to follow established lo/to procedures. Corrective actions included suspension of the responsible foreman and a reemphasisation on the importance of morning meetings with all contractor and supervisory personnel to review and/or define the daily work plans, review any permitting requirements for the job and the enforcement of group lo/to procedures.
Report Received Date 2013-05-21 00:00:00
Iyear 2013
Report Number 20130174
Supplemental Number 18801
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-04-23 11:30:00
Location Latitude 32.0711 Google Maps OpenStreetMap
Location Longitude -96.47409 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2013-04-23 11:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain System Was Not Operating At The Time.
On Site Datetime 2013-04-23 11:35:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Corsicana Tank Farm
Segment Name Ringgold 16" Inbound Meter Setting
Onshore State Abbreviation Tx
Onshore Postal Code 75110
Onshore City Name Corsicana
Onshore County Name Navarro
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Relief Line And Relief Equipment
Release Type Other
Release Type Details A Third Party Electrical Contractor Removed A Flow Switch From An Active Surge Relief Line.
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 343
Est Cost Prop Damage 50
Est Cost Emergency 500
Est Cost Environmental 23122
Est Cost Other 0
Prpty 24015
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Specialist
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 281-637-6425
Prepared Date 2013-12-06 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Specialist
Authorizer Email T*********@s**************.com
Narrative On 4/23/2013 a release occurred at the corsicana meter setting when a third party electrical contractor removed a flow switch from an active surge relief line. The subsequent investigation revealed that the contractor acted independently and performed unauthorized/unapproved work and in doing so also failed to follow established lo/to procedures. Corrective actions included suspension of the responsible foreman and a reemphasisation on the importance of morning meetings with all contractor and supervisory personnel to review and/or define the daily work plans, review any permitting requirements for the job and the enforcement of group lo/to procedures.

All rights reserved. Copyright © by ClearPHMSA