Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2013-04-19 — TX
Operator
Rose Rock Midstream L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$5,000
Incident datetime
2013-04-19 11:00
Report number
Location
TX
Narrative
Small leak occurred due to internal corrosion in an idled portion of pipeline. Pipeline has been displaced with nitrogen and line capped.
Detailed record list
Report Received Date
2013-05-16 00:00:00
Iyear
2013
Report Number
20130171
Supplemental Number
18289
Report Type
Supplemental
Operator Id
31476
Name
Rose Rock Midstream L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-04-19 11:00:00
Location Latitude
36.54755
Location Longitude
-97.20423
Commodity Released Type
Crude Oil
Unintentional Release Bbls
3
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-04-19 11:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-04-19 11:00:00
Restart Datetime
2013-04-19 19:00:00
On Site Datetime
2013-04-19 11:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
West Ponca Truck Station
Segment Name
Fiske 8" Line
Onshore State Abbreviation
Ok
Onshore Postal Code
74601
Onshore County Name
Kay
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Release Type
Leak
Leak Type
Pinhole
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
4000
Est Cost Gas Released
200
Est Cost Prop Damage
5000
Est Cost Emergency
1500
Est Cost Environmental
1700
Est Cost Other
0
Prpty
12400
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Preparer Name
E**** C***
Preparer Title
Director Ehs And Dot Compliance
Preparer Email
E****@s***********.com
Preparer Telephone
9186403384
Preparer Fax
9185247243
Prepared Date
2013-07-16 00:00:00
Authorizer Name
E**** C***
Authorizer Telephone
9186403384
Authorizer Title
Director Ehs And Dot Compliance
Authorizer Email
E****@s***********.com
Narrative
Small leak occurred due to internal corrosion in an idled portion of pipeline. Pipeline has been displaced with nitrogen and line capped.
| Report Received Date | 2013-05-16 00:00:00 |
|---|---|
| Iyear | 2013 |
| Report Number | 20130171 |
| Supplemental Number | 18289 |
| Report Type | Supplemental |
| Operator Id | 31476 PHMSA Enforcement |
| Name | Rose Rock Midstream L.p. |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2013-04-19 11:00:00 |
| Location Latitude | 36.54755 Google Maps OpenStreetMap |
| Location Longitude | -97.20423 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 3 |
| Recovered Bbls | 1 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2013-04-19 11:00:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2013-04-19 11:00:00 |
| Restart Datetime | 2013-04-19 19:00:00 |
| On Site Datetime | 2013-04-19 11:30:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | West Ponca Truck Station |
| Segment Name | Fiske 8" Line |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 74601 |
| Onshore County Name | Kay |
| Federal | No |
| Location Type | Pipeline Right-Of-Way |
| Incident Area Type | Underground |
| Pipe Facility Type | Intrastate |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Release Type | Leak |
| Leak Type | Pinhole |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 4000 |
| Est Cost Gas Released | 200 |
| Est Cost Prop Damage | 5000 |
| Est Cost Emergency | 1500 |
| Est Cost Environmental | 1700 |
| Est Cost Other | 0 |
| Prpty | 12400 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | Internal Corrosion |
| Internal External | Internal Corrosion |
| Preparer Name | E**** C*** |
| Preparer Title | Director Ehs And Dot Compliance |
| Preparer Email | E****@s***********.com |
| Preparer Telephone | 9186403384 |
| Preparer Fax | 9185247243 |
| Prepared Date | 2013-07-16 00:00:00 |
| Authorizer Name | E**** C*** |
| Authorizer Telephone | 9186403384 |
| Authorizer Title | Director Ehs And Dot Compliance |
| Authorizer Email | E****@s***********.com |
| Narrative | Small leak occurred due to internal corrosion in an idled portion of pipeline. Pipeline has been displaced with nitrogen and line capped. |
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