HL incident on 2013-04-07 — PA

Operator
Buckeye Partners, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2013-04-07 20:15
Report number
Location
PA
Narrative
A high sump alarm was received at new haven booster #1 at 20:15 on 4/7/2013. The station was not running at the time. Local personnel arrived on site at 20:30 to investigate. Investigation revealed that the shaft seal on booster unit #1 was leaking gasoline and dripping directly into the sump drain. All released product was captured in the sump. No remediation is required. The seal will be repaired under waranty by the company that installed it.
Detailed record list
Report Received Date
2013-05-06 00:00:00
Iyear
2013
Report Number
20130161
Supplemental Number
18001
Report Type
Original Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
Five Tek Park
Operator City Name
Breinigsville
Operator State Abbreviation
PA
Operator Postal Code
18031
Local Datetime
2013-04-07 20:15:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.95
Recovered Bbls
0.95
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-04-07 20:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Facility Was Already Shut Down
On Site Datetime
2013-04-07 20:30:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Aa
Segment Name
New Haven Booster #1
Onshore State Abbreviation
Ct
Onshore Postal Code
06512
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
500
Est Cost Environmental
0
Est Cost Other
0
Prpty
500
Pipeline Function
< 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
B*** Y**********
Preparer Title
Compliance Specialist
Preparer Email
B***********@b******.com
Preparer Telephone
610-904-4958
Prepared Date
2013-05-06 00:00:00
Authorizer Name
J*** R*******
Authorizer Telephone
610-904-4185
Authorizer Title
Manager Compliance
Authorizer Email
J********@b******.com
Narrative
A high sump alarm was received at new haven booster #1 at 20:15 on 4/7/2013. The station was not running at the time. Local personnel arrived on site at 20:30 to investigate. Investigation revealed that the shaft seal on booster unit #1 was leaking gasoline and dripping directly into the sump drain. All released product was captured in the sump. No remediation is required. The seal will be repaired under waranty by the company that installed it.
Report Received Date 2013-05-06 00:00:00
Iyear 2013
Report Number 20130161
Supplemental Number 18001
Report Type Original Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address Five Tek Park
Operator City Name Breinigsville
Operator State Abbreviation PA
Operator Postal Code 18031
Local Datetime 2013-04-07 20:15:00
Location Latitude 41.2885 Google Maps OpenStreetMap
Location Longitude -72.8999 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.95
Recovered Bbls 0.95
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2013-04-07 20:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Facility Was Already Shut Down
On Site Datetime 2013-04-07 20:30:00
Ignite Ind No
Explode Ind No
Pipe Fac Name Aa
Segment Name New Haven Booster #1
Onshore State Abbreviation Ct
Onshore Postal Code 06512
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Pump
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 500
Est Cost Environmental 0
Est Cost Other 0
Prpty 500
Pipeline Function < 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Preparer Name B*** Y**********
Preparer Title Compliance Specialist
Preparer Email B***********@b******.com
Preparer Telephone 610-904-4958
Prepared Date 2013-05-06 00:00:00
Authorizer Name J*** R*******
Authorizer Telephone 610-904-4185
Authorizer Title Manager Compliance
Authorizer Email J********@b******.com
Narrative A high sump alarm was received at new haven booster #1 at 20:15 on 4/7/2013. The station was not running at the time. Local personnel arrived on site at 20:30 to investigate. Investigation revealed that the shaft seal on booster unit #1 was leaking gasoline and dripping directly into the sump drain. All released product was captured in the sump. No remediation is required. The seal will be repaired under waranty by the company that installed it.

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