HL incident on 2013-03-29 — TX

Operator
Shell Pipeline Co., L.p.
Cause
Excavation Issue
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,830,000
Incident datetime
2013-03-29 10:04
Report number
Location
TX
Narrative
Cause determined by metallurgical inspection. The crack is attibuted to a bending load in the presence of an incomplete weld. Backfilling by 3rd party contractor. The pipeline failed due to forces applied to the top of the pipeline during the backfilling of the site. The quality of the weld also played a role in the incident. The weld was confirmed by analysis that it was fit-for-service. The weld did not fail due to pipeline operating pressures. Further confirmed that the weld was strong enough to withstand the maximum operating pressure (mop), hydrotest pressures and typical loads associated with the construction and maintenance of the pipeline. Locating the release - due to the recent backfilling and loose uncompacted soils at the site, the released crude oil was not discovered until the isolated section of pipeline was filled with dyed water to determine location. This was april 3rd. This added water to the uncompacted soils which displaced the crude oil to the surface and nearby bayou which was discoverd by pipeline operator crews later that day.
Detailed record list
Report Received Date
2013-04-26 00:00:00
Iyear
2013
Report Number
20130149
Supplemental Number
18747
Report Type
Supplemental Final
Operator Id
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2013-03-29 10:04:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
940
Recovered Bbls
525
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2013-03-29 10:04:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-03-29 10:04:00
Restart Datetime
2013-05-30 14:00:00
On Site Datetime
2013-03-29 11:00:00
Nrc Rpt Datetime
2013-03-30 13:04:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
East Houston To West Columbia 16"
Segment Name
East Houston To Shaver Junction 16"
Onshore State Abbreviation
Tx
Onshore Postal Code
77502
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Survey Station No.
Designated Name
491+18
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
96
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
16
Pipe Wall Thickness
0.281
Pipe Smys
46000
Pipe Specification
5l-X
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Youngstown
Pipe Coating Type
Coal Tar
Weld Subtype
Pipe Girth Weld
Installation Year
1949
Manufactured Year
1948
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
Yes
Fish Aquatic Impact Ind
Yes
Birds Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
66
Rel Water Name
Vince Bayou
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
60000
Est Cost Prop Damage
1830000
Est Cost Emergency
3110000
Est Cost Environmental
5000000
Est Cost Other
0
Prpty
10000000
Accident Psig
0
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
3469
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was detected by cpm tools upon startup of the pipeline. The controller's actions could not have contributed to the release because there were no actions taken to cause a surge, overpressure or abnormal condition. The controller executed a type 1 shutdown. The controller's response to the line balance alarm was timely and the shutdown was executed per procedure.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Easement
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Liquid Pipeline
One Call Notified Ind
Yes
One Call Ticket Num
1354383689
One Call Center Name
Lonestar
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
1440
Root Cause Category
Excavation Issue
Root Cause Type
Improper Backfilling Practices
Preparer Name
R****** K*****
Preparer Title
Regulatory Specialist
Preparer Email
R*************@s****.com
Preparer Telephone
713 241 1064
Prepared Date
2013-11-20 00:00:00
Authorizer Name
B**** S*******
Authorizer Telephone
713 241 3620
Authorizer Title
Integrity And Regulatory Manager
Authorizer Email
B*************@s****.com
Narrative
Cause determined by metallurgical inspection. The crack is attibuted to a bending load in the presence of an incomplete weld. Backfilling by 3rd party contractor. The pipeline failed due to forces applied to the top of the pipeline during the backfilling of the site. The quality of the weld also played a role in the incident. The weld was confirmed by analysis that it was fit-for-service. The weld did not fail due to pipeline operating pressures. Further confirmed that the weld was strong enough to withstand the maximum operating pressure (mop), hydrotest pressures and typical loads associated with the construction and maintenance of the pipeline. Locating the release - due to the recent backfilling and loose uncompacted soils at the site, the released crude oil was not discovered until the isolated section of pipeline was filled with dyed water to determine location. This was april 3rd. This added water to the uncompacted soils which displaced the crude oil to the surface and nearby bayou which was discoverd by pipeline operator crews later that day.
Report Received Date 2013-04-26 00:00:00
Iyear 2013
Report Number 20130149
Supplemental Number 18747
Report Type Supplemental Final
Operator Id 31174 PHMSA Enforcement
Name Shell Pipeline Co., L.p.
Operator Street Address 150 North Dairy Ashford Road Wck Bldg. A
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2013-03-29 10:04:00
Location Latitude 29.716111 Google Maps OpenStreetMap
Location Longitude -95.2219583 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 940
Recovered Bbls 525
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2013-03-29 10:04:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-03-29 10:04:00
Restart Datetime 2013-05-30 14:00:00
On Site Datetime 2013-03-29 11:00:00
Nrc Rpt Datetime 2013-03-30 13:04:00
Nrc Rpt Num 1042526 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name East Houston To West Columbia 16"
Segment Name East Houston To Shaver Junction 16"
Onshore State Abbreviation Tx
Onshore Postal Code 77502
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Survey Station No.
Designated Name 491+18
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 96
Crossing No
Pipe Facility Type Intrastate
Item Involved Weld, Including Heat-Affected Zone
Pipe Diameter 16
Pipe Wall Thickness 0.281
Pipe Smys 46000
Pipe Specification 5l-X
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Youngstown
Pipe Coating Type Coal Tar
Weld Subtype Pipe Girth Weld
Installation Year 1949
Manufactured Year 1948
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind Yes
Fish Aquatic Impact Ind Yes
Birds Impact Ind Yes
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 66
Rel Water Name Vince Bayou
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 60000
Est Cost Prop Damage 1830000
Est Cost Emergency 3110000
Est Cost Environmental 5000000
Est Cost Other 0
Prpty 10000000
Accident Psig 0
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 3469
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was detected by cpm tools upon startup of the pipeline. The controller's actions could not have contributed to the release because there were no actions taken to cause a surge, overpressure or abnormal condition. The controller executed a type 1 shutdown. The controller's response to the line balance alarm was timely and the shutdown was executed per procedure.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Easement
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Liquid Pipeline
One Call Notified Ind Yes
One Call Ticket Num 1354383689
One Call Center Name Lonestar
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 1440
Root Cause Category Excavation Issue
Root Cause Type Improper Backfilling Practices
Preparer Name R****** K*****
Preparer Title Regulatory Specialist
Preparer Email R*************@s****.com
Preparer Telephone 713 241 1064
Prepared Date 2013-11-20 00:00:00
Authorizer Name B**** S*******
Authorizer Telephone 713 241 3620
Authorizer Title Integrity And Regulatory Manager
Authorizer Email B*************@s****.com
Narrative Cause determined by metallurgical inspection. The crack is attibuted to a bending load in the presence of an incomplete weld. Backfilling by 3rd party contractor. The pipeline failed due to forces applied to the top of the pipeline during the backfilling of the site. The quality of the weld also played a role in the incident. The weld was confirmed by analysis that it was fit-for-service. The weld did not fail due to pipeline operating pressures. Further confirmed that the weld was strong enough to withstand the maximum operating pressure (mop), hydrotest pressures and typical loads associated with the construction and maintenance of the pipeline. Locating the release - due to the recent backfilling and loose uncompacted soils at the site, the released crude oil was not discovered until the isolated section of pipeline was filled with dyed water to determine location. This was april 3rd. This added water to the uncompacted soils which displaced the crude oil to the surface and nearby bayou which was discoverd by pipeline operator crews later that day.

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