HL incident on 2013-03-27 — TX

Operator
Energy Transfer Company
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,100
Incident datetime
2013-03-27 09:15
Report number
Location
TX
Narrative
At 0840 hrs. On march 27, 2013 a third party representative contacted etc's liquids control center to report a small vapor leak located off of fm 626 at etc's kenedy lateral tap location. Employee with etc operations was informed of the leak and was dispatched to investigate. He arrived at 0915 hrs. On same day, to investigate and verified that there was a small leak on etc's facility. It was determined that the leak was a minimal hazard with no immediate threat to the public, property, or environment. Appropriate notifications were made. The site was monitored until contractors and repair materials arrived on location at 1300 hrs. At 1326 hrs. The check valve was isolated and blown down. It was removed and replaced and the line was returned to service at 1554 hrs on march 27, 2013. Final update: nov. 8, 2013 all damages were limited to lost product and repairs to the leaking seals. Estimated cost noted on initial report remain accurate. Cpm leak detection is now installed on the kennedy lateral and is fully functional. The check valve was modified with a different type of external packing gland to prevent similiar reoccurrences.
Detailed record list
Report Received Date
2013-04-23 00:00:00
Iyear
2013
Report Number
20130144
Supplemental Number
18712
Report Type
Supplemental Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-03-27 09:15:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
5.88
Intentional Release Bbls
6.78
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2013-03-27 09:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-03-27 13:26:00
Restart Datetime
2013-03-27 15:54:00
On Site Datetime
2013-03-27 09:15:00
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Kenedy Tap Site
Segment Name
Kenedy Tap Site
Onshore State Abbreviation
Tx
Onshore Postal Code
78118
Onshore City Name
Kenedy
Onshore County Name
Karnes
Designated Location
Milepost/valve Station
Designated Name
5.12
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Check
Valve Manufacturer
Wheatley
Installation Year
2012
Manufactured Year
2012
Material Involved
Material Other Than Carbon Steel
Material Details
O" Ring Seal On Check Valve Flapper Rod
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
300
Est Cost Prop Damage
2100
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Est Cost Other Details
A Small Ngl Leak Was Discovered On A Seal, On The Flapper Of A Check Valve.
Prpty
2400
Accident Psig
980
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
50
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak was so minor that there was no pressure differential and cause was apparrant relating to the seal on the check valve.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
0" Ring On Flapper Support Shaft Failed
Eq Additional Other Ind
Yes
Eq Additional Other Details
Seals On Shaft Could Not Accommodate The Throttling Of Operating Environment
Preparer Name
D**** N******
Preparer Title
Director Regulatory Compliance
Preparer Email
D************@e*************.com
Preparer Telephone
832.668.1006
Preparer Fax
832.668.1129
Prepared Date
2013-11-08 00:00:00
Authorizer Name
D**** N******
Authorizer Telephone
832.668.1006
Authorizer Title
Director Regulatory Compliance
Authorizer Email
D************@e*************.com
Narrative
At 0840 hrs. On march 27, 2013 a third party representative contacted etc's liquids control center to report a small vapor leak located off of fm 626 at etc's kenedy lateral tap location. Employee with etc operations was informed of the leak and was dispatched to investigate. He arrived at 0915 hrs. On same day, to investigate and verified that there was a small leak on etc's facility. It was determined that the leak was a minimal hazard with no immediate threat to the public, property, or environment. Appropriate notifications were made. The site was monitored until contractors and repair materials arrived on location at 1300 hrs. At 1326 hrs. The check valve was isolated and blown down. It was removed and replaced and the line was returned to service at 1554 hrs on march 27, 2013. Final update: nov. 8, 2013 all damages were limited to lost product and repairs to the leaking seals. Estimated cost noted on initial report remain accurate. Cpm leak detection is now installed on the kennedy lateral and is fully functional. The check valve was modified with a different type of external packing gland to prevent similiar reoccurrences.
Report Received Date 2013-04-23 00:00:00
Iyear 2013
Report Number 20130144
Supplemental Number 18712
Report Type Supplemental Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-03-27 09:15:00
Location Latitude 28.8239 Google Maps OpenStreetMap
Location Longitude -97.9906 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 5.88
Intentional Release Bbls 6.78
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2013-03-27 09:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-03-27 13:26:00
Restart Datetime 2013-03-27 15:54:00
On Site Datetime 2013-03-27 09:15:00
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Kenedy Tap Site
Segment Name Kenedy Tap Site
Onshore State Abbreviation Tx
Onshore Postal Code 78118
Onshore City Name Kenedy
Onshore County Name Karnes
Designated Location Milepost/valve Station
Designated Name 5.12
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Check
Valve Manufacturer Wheatley
Installation Year 2012
Manufactured Year 2012
Material Involved Material Other Than Carbon Steel
Material Details O" Ring Seal On Check Valve Flapper Rod
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 300
Est Cost Prop Damage 2100
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Est Cost Other Details A Small Ngl Leak Was Discovered On A Seal, On The Flapper Of A Check Valve.
Prpty 2400
Accident Psig 980
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 50
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak was so minor that there was no pressure differential and cause was apparrant relating to the seal on the check valve.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details 0" Ring On Flapper Support Shaft Failed
Eq Additional Other Ind Yes
Eq Additional Other Details Seals On Shaft Could Not Accommodate The Throttling Of Operating Environment
Preparer Name D**** N******
Preparer Title Director Regulatory Compliance
Preparer Email D************@e*************.com
Preparer Telephone 832.668.1006
Preparer Fax 832.668.1129
Prepared Date 2013-11-08 00:00:00
Authorizer Name D**** N******
Authorizer Telephone 832.668.1006
Authorizer Title Director Regulatory Compliance
Authorizer Email D************@e*************.com
Narrative At 0840 hrs. On march 27, 2013 a third party representative contacted etc's liquids control center to report a small vapor leak located off of fm 626 at etc's kenedy lateral tap location. Employee with etc operations was informed of the leak and was dispatched to investigate. He arrived at 0915 hrs. On same day, to investigate and verified that there was a small leak on etc's facility. It was determined that the leak was a minimal hazard with no immediate threat to the public, property, or environment. Appropriate notifications were made. The site was monitored until contractors and repair materials arrived on location at 1300 hrs. At 1326 hrs. The check valve was isolated and blown down. It was removed and replaced and the line was returned to service at 1554 hrs on march 27, 2013. Final update: nov. 8, 2013 all damages were limited to lost product and repairs to the leaking seals. Estimated cost noted on initial report remain accurate. Cpm leak detection is now installed on the kennedy lateral and is fully functional. The check valve was modified with a different type of external packing gland to prevent similiar reoccurrences.

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