GD incident on 2013-08-14 — MA

Operator
Boston Gas Co
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$68,000
Incident datetime
2013-08-14 15:40
Report number
Location
MA, MIDDLESEX
Narrative
The event occurred during a reinforcement project requiring the replacement of approx. 2800ft of existing 3'/4' coated steel and plastic main with an 8'plastic pipe at high pressure (60psi) and associated tie-ins along middlesex turnpike, bedford, ma. The new 8' main was installed by new england utility constructors inc. (neuco) with gassing in and associated tie-ins performed by a national grid crew. On august 14, 2013, during the operation by a national grid's crew to tie-in the existing 8' main on plank street to the new 8' main on middlesex turnpike, the crew leader released the pressure on the hydraulic squeeze off at one end of the tie-in prior making the connection at the other end. This resulted in an uncontrolled release of gas through the open ended pipe which ignited and burned for approx. 70 minutes before being brought under control and extinguished there was no loss of life or significant injury but there was damage to third party apparatus in the vicinity including overhead wires and street lighting and company equipment including a back hoe. There was significant media attention
Detailed record list
Occurred At
2013-08-14 15:40:00
Year
2013
Report Received Date
2013-09-13 00:00:00
Iyear
2013.0
Report Number
20130103.0
Supplemental Number
30401.0
Report Type
Supplemental Final
Operator Id
Name
Boston Gas Co
Operator Street Address
170 Data Drive
Operator City Name
Waltham
Operator State Abbreviation
MA
Operator Postal Code
02451
Local Datetime
2013-08-14 15:40:00
Location Street Address
Plank Street & Middlesex Turnpike
Location City Name
Bedford
Location County Name
Middlesex
Location State Abbreviation
MA
Location Postal Code
01730
Location Latitude
Location Longitude
Nrc Rpt Datetime
2013-08-14 17:31:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
221.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2013-08-14 15:40:00
On Site Datetime
2013-08-14 15:40:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
2013.0
Pipe Diameter
8.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Chevron Philips Chemical Co.
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
13.5
Material Pe Pipe Code
2406
Release Type
Other
Release Type Details
Natural Gas Was Introduced Into 8 Inch Plastic Main Prior To Completion Of Tie-In
Class Location Type
Class 4 Location
Est Cost Oper Paid
25000.0
Est Cost Prop Damage
68000.0
Est Cost Emergency
15700.0
Est Cost Other
0.0
Est Cost Unintentional Release
751.0
Prpty
109451.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
55.2
Normal Psig
60.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Num Employees Tested
3
Num Employees Failed
0
Contractor Drug Test Ind
Yes
Num Contractors Tested
4
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Crew Leader Released The Pressure On The Hydraulic Squeeze Off Tool At One End Of The Tie-In Prior To Making Connection At Other End. This Resulted In An Uncontrolled Release Of Gas.
Related Failure Follow Ind
Yes
Category Type
Construction
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
K******* M*******
Preparer Title
Manager Dispatch
Preparer Email
K**********************@us.n****.com
Preparer Telephone
508-421-7450
Authorizer Name
C****** D B*****
Authorizer Title
Principal Program Manager Federal Programs
Authorizer Telephone
6317703549
Authorizer Email
C*************@n***********.com
Narrative
The event occurred during a reinforcement project requiring the replacement of approx. 2800ft of existing 3'/4' coated steel and plastic main with an 8'plastic pipe at high pressure (60psi) and associated tie-ins along middlesex turnpike, bedford, ma. The new 8' main was installed by new england utility constructors inc. (neuco) with gassing in and associated tie-ins performed by a national grid crew. On august 14, 2013, during the operation by a national grid's crew to tie-in the existing 8' main on plank street to the new 8' main on middlesex turnpike, the crew leader released the pressure on the hydraulic squeeze off at one end of the tie-in prior making the connection at the other end. This resulted in an uncontrolled release of gas through the open ended pipe which ignited and burned for approx. 70 minutes before being brought under control and extinguished there was no loss of life or significant injury but there was damage to third party apparatus in the vicinity including overhead wires and street lighting and company equipment including a back hoe. There was significant media attention
Occurred At 2013-08-14 15:40:00
Year 2013
Report Received Date 2013-09-13 00:00:00
Iyear 2013.0
Report Number 20130103.0
Supplemental Number 30401.0
Report Type Supplemental Final
Operator Id 1640 PHMSA Enforcement
Name Boston Gas Co
Operator Street Address 170 Data Drive
Operator City Name Waltham
Operator State Abbreviation MA
Operator Postal Code 02451
Local Datetime 2013-08-14 15:40:00
Location Street Address Plank Street & Middlesex Turnpike
Location City Name Bedford
Location County Name Middlesex
Location State Abbreviation MA
Location Postal Code 01730
Location Latitude 42.51515 Google Maps OpenStreetMap
Location Longitude -71.241569 Google Maps OpenStreetMap
Nrc Rpt Datetime 2013-08-14 17:31:00
Nrc Rpt Num 1057121 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 221.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2013-08-14 15:40:00
On Site Datetime 2013-08-14 15:40:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 2013.0
Pipe Diameter 8.0
Pipe Specification Astm D2513
Pipe Manufacturer Chevron Philips Chemical Co.
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 13.5
Material Pe Pipe Code 2406
Release Type Other
Release Type Details Natural Gas Was Introduced Into 8 Inch Plastic Main Prior To Completion Of Tie-In
Class Location Type Class 4 Location
Est Cost Oper Paid 25000.0
Est Cost Prop Damage 68000.0
Est Cost Emergency 15700.0
Est Cost Other 0.0
Est Cost Unintentional Release 751.0
Prpty 109451.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 55.2
Normal Psig 60.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind Yes
Num Employees Tested 3
Num Employees Failed 0
Contractor Drug Test Ind Yes
Num Contractors Tested 4
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Crew Leader Released The Pressure On The Hydraulic Squeeze Off Tool At One End Of The Tie-In Prior To Making Connection At Other End. This Resulted In An Uncontrolled Release Of Gas.
Related Failure Follow Ind Yes
Category Type Construction
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name K******* M*******
Preparer Title Manager Dispatch
Preparer Email K**********************@us.n****.com
Preparer Telephone 508-421-7450
Authorizer Name C****** D B*****
Authorizer Title Principal Program Manager Federal Programs
Authorizer Telephone 6317703549
Authorizer Email C*************@n***********.com
Narrative The event occurred during a reinforcement project requiring the replacement of approx. 2800ft of existing 3'/4' coated steel and plastic main with an 8'plastic pipe at high pressure (60psi) and associated tie-ins along middlesex turnpike, bedford, ma. The new 8' main was installed by new england utility constructors inc. (neuco) with gassing in and associated tie-ins performed by a national grid crew. On august 14, 2013, during the operation by a national grid's crew to tie-in the existing 8' main on plank street to the new 8' main on middlesex turnpike, the crew leader released the pressure on the hydraulic squeeze off at one end of the tie-in prior making the connection at the other end. This resulted in an uncontrolled release of gas through the open ended pipe which ignited and burned for approx. 70 minutes before being brought under control and extinguished there was no loss of life or significant injury but there was damage to third party apparatus in the vicinity including overhead wires and street lighting and company equipment including a back hoe. There was significant media attention

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