Incident details
Operator, cause, commodity and consequences with raw source fields.
GTG incident on 2013-08-20 — TX
Operator
Enable Oklahoma Intrastate Transmission, Llc
Cause
Miscellaneous Root Causes
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$40,000
Incident datetime
2013-08-20 11:05
Report number
Location
TX
Narrative
Mcalester line 263 ruptured just south of kiowa in a pasture causing a grass/timber fire. Local fire department and local authorities arrived on scene to assist. No injuries and no structures were involved. The pipeline fire dissipated from shutting the gas in and fire department was able to control fire and keep it from spreading. The damaged section of pipe was removed and showed signs of third-party damage. It has been sent to a metallurgist for further analysis and we are awaiting the results. Note: the damaged section of pipe was replaced. A gauge pig was ran on 8/22/13 before pipeline was placed back into service. Supplemental information. The metallurgist report concluded that the third party damage resulted in: fracture initiated on a damaged area of the pipeline where deep gouge marks were noted on the outside surface. There were two parallel scrape marks running roughly in the longitudinal direction and produced considerable deformation of the steel. Final failure of the pipeline was a result of ductile overload. External damage and necking had resulted in a wall thickness reduced to approximately 0.160" from the measured 0.225" undamaged wall nearby. The undamaged section of pipe was tested and met all the requirements of API specification 5l, psl 2, grade x52.
Detailed record list
Report Received Date
2013-09-19 00:00:00
Iyear
2013
Report Number
20130088
Supplemental Number
16282
Report Type
Supplemental Final
Operator Id
26330
Name
Enable Oklahoma Intrastate Transmission, Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-08-20 11:05:00
Location Latitude
34.695189
Location Longitude
-95.919508
Nrc Rpt Num
1057718
Nrc Rpt Datetime
2013-08-20 18:20:00
Commodity Released Type
Natural Gas
Unintentional Release
5100
Intentional Release
680
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-08-20 11:22:00
Restart Datetime
2013-08-22 10:00:00
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2013-08-20 11:05:00
On Site Datetime
2013-08-20 11:25:00
On Off Shore
Onshore
Onshore State Abbreviation
Ok
Onshore Postal Code
74553
Onshore City Name
Kiowa
Onshore County Name
Pittsburg County
Designated Location
Milepost
Pipe Fac Name
L-263
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.219
Pipe Smys
52000
Pipe Specification
Longitudinal Erw- High Frequency
Pipe Seam Type
Longitudinal Erw - High Frequency
Pipe Manufacturer
Lone Star Steel
Pipe Coating Type
Epoxy
Installation Year
2007
Manufactured Year
2007
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
36
Rupture Width
12
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
305
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
13500
Est Cost Unintentional Release
17000
Est Cost Intentional Release
2300
Est Cost Prop Damage
40000
Est Cost Emergency
3000
Est Cost Other
0
Prpty
75800
Accident Psig
1120
Mop Psig
1200
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
50160
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pipe showing signs of third party damage
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Previous Damage Due To Excavation Activity
Ex Party Type
Previous Damage Due To Excavation Activity
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Excavator Type
Unknown/other
Excavator Equipment
Unknown/other
Work Performed
Unknown/other
One Call Notified Ind
No
Locator Type
Unknown/other
Visible Marks
No
Service Interruption
No
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Previous Damage
Collected Data Ind
No
Insp Compl Before Damage Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
P****** K*****
Preparer Title
Dot Compliance Coordinator
Preparer Email
K*************@e*****.com
Preparer Telephone
9186883330
Authorizer Name
P*** M B*****
Authorizer Title
V.p. Operations
Authorizer Telephone
4055257788
Authorizer Email
No Email Address
Narrative
Mcalester line 263 ruptured just south of kiowa in a pasture causing a grass/timber fire. Local fire department and local authorities arrived on scene to assist. No injuries and no structures were involved. The pipeline fire dissipated from shutting the gas in and fire department was able to control fire and keep it from spreading. The damaged section of pipe was removed and showed signs of third-party damage. It has been sent to a metallurgist for further analysis and we are awaiting the results. Note: the damaged section of pipe was replaced. A gauge pig was ran on 8/22/13 before pipeline was placed back into service. Supplemental information. The metallurgist report concluded that the third party damage resulted in: fracture initiated on a damaged area of the pipeline where deep gouge marks were noted on the outside surface. There were two parallel scrape marks running roughly in the longitudinal direction and produced considerable deformation of the steel. Final failure of the pipeline was a result of ductile overload. External damage and necking had resulted in a wall thickness reduced to approximately 0.160" from the measured 0.225" undamaged wall nearby. The undamaged section of pipe was tested and met all the requirements of API specification 5l, psl 2, grade x52.
| Report Received Date | 2013-09-19 00:00:00 |
|---|---|
| Iyear | 2013 |
| Report Number | 20130088 |
| Supplemental Number | 16282 |
| Report Type | Supplemental Final |
| Operator Id | 26330 PHMSA Enforcement |
| Name | Enable Oklahoma Intrastate Transmission, Llc |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2013-08-20 11:05:00 |
| Location Latitude | 34.695189 Google Maps OpenStreetMap |
| Location Longitude | -95.919508 Google Maps OpenStreetMap |
| Nrc Rpt Num | 1057718 NRC Report How to search |
| Nrc Rpt Datetime | 2013-08-20 18:20:00 |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 5100 |
| Intentional Release | 680 |
| Accompanying Liquid | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2013-08-20 11:22:00 |
| Restart Datetime | 2013-08-22 10:00:00 |
| Ignite Ind | Yes |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Incident Identified Datetime | 2013-08-20 11:05:00 |
| On Site Datetime | 2013-08-20 11:25:00 |
| On Off Shore | Onshore |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 74553 |
| Onshore City Name | Kiowa |
| Onshore County Name | Pittsburg County |
| Designated Location | Milepost |
| Pipe Fac Name | L-263 |
| Federal | No |
| Location Type | Pipeline Right-Of-Way |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 36 |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Pipe Diameter | 12 |
| Pipe Wall Thickness | 0.219 |
| Pipe Smys | 52000 |
| Pipe Specification | Longitudinal Erw- High Frequency |
| Pipe Seam Type | Longitudinal Erw - High Frequency |
| Pipe Manufacturer | Lone Star Steel |
| Pipe Coating Type | Epoxy |
| Installation Year | 2007 |
| Manufactured Year | 2007 |
| Material Involved | Carbon Steel |
| Release Type | Rupture |
| Rupture Orient | Circumferential |
| Rupture Length | 36 |
| Rupture Width | 12 |
| Class Location Type | Class 1 Location |
| Could Be Hca | No |
| Pir Radius | 305 |
| Heat Damage Ind | No |
| Non Heat Damage Ind | No |
| Hca Fatalities Ind | No |
| Est Cost Oper Paid | 13500 |
| Est Cost Unintentional Release | 17000 |
| Est Cost Intentional Release | 2300 |
| Est Cost Prop Damage | 40000 |
| Est Cost Emergency | 3000 |
| Est Cost Other | 0 |
| Prpty | 75800 |
| Accident Psig | 1120 |
| Mop Psig | 1200 |
| Mop Cfr Section | Not On Omb-Approved Form When Submitted View CFR 49 §192 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Pressure Restriction Ind | No |
| Upstream Valve Type Ind | Manual |
| Downstream Valve Type Ind | Manual |
| Length Segment Isolated | 50160 |
| Internal Inspection Ind | Yes |
| Operation Complications Ind | No |
| Pipeline Function | Transmission System |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | Yes |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Pipe showing signs of third party damage |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Excavation Damage |
| Cause Details | Previous Damage Due To Excavation Activity |
| Ex Party Type | Previous Damage Due To Excavation Activity |
| Notify Cga Dirt | No |
| Private Row Ind | Yes |
| Private Subtype | Private Landowner |
| Excavator Type | Unknown/other |
| Excavator Equipment | Unknown/other |
| Work Performed | Unknown/other |
| One Call Notified Ind | No |
| Locator Type | Unknown/other |
| Visible Marks | No |
| Service Interruption | No |
| Root Cause Category | Miscellaneous Root Causes |
| Root Cause Type | Previous Damage |
| Collected Data Ind | No |
| Insp Compl Before Damage Ind | No |
| Has Hydrtst Conduc Before Ind | No |
| Direct Asmnt Conducted | No |
| Non Destructive Exam Ind | No |
| Preparer Name | P****** K***** |
| Preparer Title | Dot Compliance Coordinator |
| Preparer Email | K*************@e*****.com |
| Preparer Telephone | 9186883330 |
| Authorizer Name | P*** M B***** |
| Authorizer Title | V.p. Operations |
| Authorizer Telephone | 4055257788 |
| Authorizer Email | No Email Address |
| Narrative | Mcalester line 263 ruptured just south of kiowa in a pasture causing a grass/timber fire. Local fire department and local authorities arrived on scene to assist. No injuries and no structures were involved. The pipeline fire dissipated from shutting the gas in and fire department was able to control fire and keep it from spreading. The damaged section of pipe was removed and showed signs of third-party damage. It has been sent to a metallurgist for further analysis and we are awaiting the results. Note: the damaged section of pipe was replaced. A gauge pig was ran on 8/22/13 before pipeline was placed back into service. Supplemental information. The metallurgist report concluded that the third party damage resulted in: fracture initiated on a damaged area of the pipeline where deep gouge marks were noted on the outside surface. There were two parallel scrape marks running roughly in the longitudinal direction and produced considerable deformation of the steel. Final failure of the pipeline was a result of ductile overload. External damage and necking had resulted in a wall thickness reduced to approximately 0.160" from the measured 0.225" undamaged wall nearby. The undamaged section of pipe was tested and met all the requirements of API specification 5l, psl 2, grade x52. |
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