Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2013-06-29 — TX
Operator
Atmos Energy Corporation - Mid-Tex
Cause
Notification Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$2,174
Incident datetime
2013-06-29 16:06
Report number
Location
TX, DALLAS
Narrative
Homeowner/excavator was digging in yard with a backhoe and damaged the gas service line. The single service at 901 nw 7th in grand prairie, tx was terminated at the main and will not be restored, so no supplemental report will be required (part a, item 13.B).
Detailed record list
Occurred At
2013-06-29 16:06:00
Year
2013
Report Received Date
2013-07-29 00:00:00
Iyear
2013.0
Report Number
20130087.0
Supplemental Number
15701.0
Report Type
Original Final
Operator Id
31348
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2013-06-29 15:30:00
Location Street Address
901 Nw 7th
Location City Name
Grand Prairie
Location County Name
Dallas
Location State Abbreviation
TX
Location Postal Code
75050
Location Latitude
32.45059
Location Longitude
-97.00451
Nrc Rpt Datetime
2013-06-29 17:18:00
Nrc Rpt Num
1052202
Commodity Released Type
Natural Gas
Unintentional Release
2.19
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2013-06-29 16:06:00
On Site Datetime
2013-06-29 16:45:00
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
12.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Service
Installation Year
1982.0
Pipe Diameter
0.5
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Wt Plastic Unknown Ind
Unknown
Material Pe Pipe Code
Unknown
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
0.5
Class Location Type
Class 3 Location
Est Cost Oper Paid
100000.0
Est Cost Prop Damage
2174.0
Est Cost Emergency
0.0
Est Cost Other
0.0
Est Cost Unintentional Release
12.0
Prpty
102186.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
22.0
Normal Psig
22.0
Mop Psig
50.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Excavator Type
Occupant
Excavator Equipment
Backhoe/trackhoe
Work Performed
Drainage
One Call Notified Ind
No
Locator Type
Data Not Collected
Visible Marks
Data Not Collected
Service Interruption
Yes
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
K** P****
Preparer Title
Operations Manager
Preparer Email
K********@a**********.com
Preparer Telephone
214-316-4911
Preparer Fax
817-375-7979
Authorizer Name
M*** C******
Authorizer Title
Compliance Director
Authorizer Telephone
214-206-2875
Authorizer Email
M*************@a**********.com
Narrative
Homeowner/excavator was digging in yard with a backhoe and damaged the gas service line. The single service at 901 nw 7th in grand prairie, tx was terminated at the main and will not be restored, so no supplemental report will be required (part a, item 13.B).
| Occurred At | 2013-06-29 16:06:00 |
|---|---|
| Year | 2013 |
| Report Received Date | 2013-07-29 00:00:00 |
| Iyear | 2013.0 |
| Report Number | 20130087.0 |
| Supplemental Number | 15701.0 |
| Report Type | Original Final |
| Operator Id | 31348 PHMSA Enforcement |
| Name | Atmos Energy Corporation - Mid-Tex |
| Operator Street Address | 5430 Lbj Freeway Suite 1800 |
| Operator City Name | Dallas |
| Operator State Abbreviation | TX |
| Operator Postal Code | 75240 |
| Local Datetime | 2013-06-29 15:30:00 |
| Location Street Address | 901 Nw 7th |
| Location City Name | Grand Prairie |
| Location County Name | Dallas |
| Location State Abbreviation | TX |
| Location Postal Code | 75050 |
| Location Latitude | 32.45059 Google Maps OpenStreetMap |
| Location Longitude | -97.00451 Google Maps OpenStreetMap |
| Nrc Rpt Datetime | 2013-06-29 17:18:00 |
| Nrc Rpt Num | 1052202 NRC Report How to search |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 2.19 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Ignite Ind | Yes |
| Explode Ind | No |
| Num Pub Evacuated | 0.0 |
| Incident Identified Datetime | 2013-06-29 16:06:00 |
| On Site Datetime | 2013-06-29 16:45:00 |
| Federal | No |
| Location Type | Private Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Exposed Due To Excavation |
| Depth Of Cover | 12.0 |
| Crossing | No |
| Pipe Facility Type | Privately Owned |
| System Part Involved | Service |
| Installation Year | 1982.0 |
| Pipe Diameter | 0.5 |
| Pipe Specification | Unknown |
| Pipe Manufacturer | Unknown |
| Material Involved | Plastic |
| Plastic Type | Polyethylene (Pe) |
| Wt Plastic Unknown Ind | Unknown |
| Material Pe Pipe Code | Unknown |
| Release Type | Rupture |
| Rupture Orient | Circumferential |
| Rupture Length | 0.5 |
| Class Location Type | Class 3 Location |
| Est Cost Oper Paid | 100000.0 |
| Est Cost Prop Damage | 2174.0 |
| Est Cost Emergency | 0.0 |
| Est Cost Other | 0.0 |
| Est Cost Unintentional Release | 12.0 |
| Prpty | 102186.0 |
| Commercial Affected | 0.0 |
| Industrial Affected | 0.0 |
| Residences Affected | 0.0 |
| Accident Psig | 22.0 |
| Normal Psig | 22.0 |
| Mop Psig | 50.0 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Scada In Place Ind | No |
| Accident Identifier | Notification From Third Party That Caused The Incident |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the incident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Excavation Damage |
| Cause Details | Excavation Damage By Third Party |
| Ex Party Type | Excavation Damage By Third Party |
| Prior Notification Ind | No |
| Notify Cga Dirt | No |
| Private Row Ind | Yes |
| Private Subtype | Private Landowner |
| Excavator Type | Occupant |
| Excavator Equipment | Backhoe/trackhoe |
| Work Performed | Drainage |
| One Call Notified Ind | No |
| Locator Type | Data Not Collected |
| Visible Marks | Data Not Collected |
| Service Interruption | Yes |
| Root Cause Category | Notification Issue |
| Root Cause Type | No Notification Made To The One-Call Center/811 |
| Preparer Name | K** P**** |
| Preparer Title | Operations Manager |
| Preparer Email | K********@a**********.com |
| Preparer Telephone | 214-316-4911 |
| Preparer Fax | 817-375-7979 |
| Authorizer Name | M*** C****** |
| Authorizer Title | Compliance Director |
| Authorizer Telephone | 214-206-2875 |
| Authorizer Email | M*************@a**********.com |
| Narrative | Homeowner/excavator was digging in yard with a backhoe and damaged the gas service line. The single service at 901 nw 7th in grand prairie, tx was terminated at the main and will not be restored, so no supplemental report will be required (part a, item 13.B). |
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