GD incident on 2013-01-14 — NY

Operator
Consolidated Edison Co Of New York
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$47,993
Incident datetime
2013-01-14 12:51
Report number
Location
NY, WESTCHESTER
Narrative
On january 13, 2013 at 22:28 the resident at 1060 knollwood rd (tg) reported an outside odor and gas distribution services (gds) responded, investigated and detected 10% over the 12" 1948 245 psi transmission main. Gas construction -emergency response force (erf) responded and investigated, detecting 95% directly over the main. The 95% reading over the transmission main was aerated and 70% quickly returned. Contingency case 40-c-1 was identified and (2) transmission valves were initially staffed. An operational plan was developed to ensure no system impact or customer loss resulted as a result of the planned isolation of regulator stations gr-484 and gr-483. At 12:51 on january 14, 2013, transmission v-40427 was closed isolating the effected segment of transmission main. Pressure was reduced to approx 60 psi and excavation operations were initiated. Around-the-clock operations continued and additional investigation and excavation was completed. Approximately 21' south of the highest reading and initial excavation, a second excavation over a 12" compression coupling was completed and investigation continued. The coupling was found not leaking. A welded repair sleeve and (2) high hats were installed. On january 16, 2013 restoration operations were initiated at 12:39 and leak survey monitored the segment as pressure was restored in 60 psi increments and no leaks were found. The segment of isolated main was returned to normal operating condition at at 205 psi. Investigation continued and at 14:27 a visible leak on a 12" transmission coupling was confirmed at the compression end seal. An operational plan was developed and the leak was monitored around-the-clock until system conditions were favorable for isolation. There was no migration toward buildings and all subsurface structures remained gas free during this period. On january 19, 2013, the segment of main from v-40427 to gr-484 was isolated and pressure reduced. The leak was fully excavated and a welded repair sleeve was installed on the leaking coupling. The welds were tested and all tests passed. Restoration operations were initiated at 18:38, and at 21:31 the segment of main from v-40427 to gr-484 was restored to full line pressure after incremental increases. No other transmission leaks were found. The supply to gr-483 was restored at 22:39 after v-34589 was opened and leak survey detected no leaks. Regulator station gr-483 was returned to service. The US DOT and nys psc were notified. This was a serious level incident. Note--this gas distribution incident report was generated to replace gas transmission incident report 20130011-15731.
Detailed record list
Occurred At
2013-01-14 12:51:00
Year
2013
Report Received Date
2013-06-04 00:00:00
Iyear
2013.0
Report Number
20130073.0
Supplemental Number
15884.0
Report Type
Supplemental Final
Operator Id
Name
Consolidated Edison Co Of New York
Operator Street Address
4 Irving Place
Operator City Name
New York
Operator State Abbreviation
NY
Operator Postal Code
10003
Local Datetime
2013-01-13 22:28:00
Location Street Address
1060 Knollwood Road
Location City Name
Town Of Greenburgh
Location County Name
Westchester
Location State Abbreviation
NY
Location Postal Code
10523
Location Latitude
Location Longitude
Nrc Rpt Datetime
2013-01-14 13:18:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
14.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2013-01-14 12:51:00
On Site Datetime
2013-01-14 12:51:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under A Building
Depth Of Cover
28.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Other
System Part Details
Onshore Pipeline, Including Valve Sites
Installation Year
1948.0
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Leak
Leak Type
Seal Or Packing
Class Location Type
Class 4 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
47993.0
Est Cost Emergency
745.0
Est Cost Other
1500.0
Est Cost Other Details
Materials
Est Cost Unintentional Release
30.0
Prpty
50268.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
205.0
Normal Psig
205.0
Mop Psig
245.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak on compression coupling resulting in no pressure drop or increased flow on scada
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Mechanical Joint Failure
Pwjf Failure Type
Mechanical Joint Failure
Mec Fitting Involved
Bolted
Mec Fitting Type
Coupling
Mec Manufacturer
Dresser
Mec Fitting Material
Other
Mec Fitting Material Detail
Materials Joined: 1st Steel, 2nd Steel
Additional Other Ind
Yes
Additional Factor Details
12" Compression Coupling Seal Packing Leak
Hydrotest Conducted Ind
No
Preparer Name
K**** F****
Preparer Title
Operations Manager-Gas Emergency Response Center
Preparer Email
F*****@c****.com
Preparer Telephone
718-319-2310
Preparer Fax
718-597-5463
Authorizer Name
V***** D******
Authorizer Title
Department Manager-Gas Emergency Response Center
Authorizer Telephone
718-319-2350
Authorizer Email
D*******@c****.com
Narrative
On january 13, 2013 at 22:28 the resident at 1060 knollwood rd (tg) reported an outside odor and gas distribution services (gds) responded, investigated and detected 10% over the 12" 1948 245 psi transmission main. Gas construction -emergency response force (erf) responded and investigated, detecting 95% directly over the main. The 95% reading over the transmission main was aerated and 70% quickly returned. Contingency case 40-c-1 was identified and (2) transmission valves were initially staffed. An operational plan was developed to ensure no system impact or customer loss resulted as a result of the planned isolation of regulator stations gr-484 and gr-483. At 12:51 on january 14, 2013, transmission v-40427 was closed isolating the effected segment of transmission main. Pressure was reduced to approx 60 psi and excavation operations were initiated. Around-the-clock operations continued and additional investigation and excavation was completed. Approximately 21' south of the highest reading and initial excavation, a second excavation over a 12" compression coupling was completed and investigation continued. The coupling was found not leaking. A welded repair sleeve and (2) high hats were installed. On january 16, 2013 restoration operations were initiated at 12:39 and leak survey monitored the segment as pressure was restored in 60 psi increments and no leaks were found. The segment of isolated main was returned to normal operating condition at at 205 psi. Investigation continued and at 14:27 a visible leak on a 12" transmission coupling was confirmed at the compression end seal. An operational plan was developed and the leak was monitored around-the-clock until system conditions were favorable for isolation. There was no migration toward buildings and all subsurface structures remained gas free during this period. On january 19, 2013, the segment of main from v-40427 to gr-484 was isolated and pressure reduced. The leak was fully excavated and a welded repair sleeve was installed on the leaking coupling. The welds were tested and all tests passed. Restoration operations were initiated at 18:38, and at 21:31 the segment of main from v-40427 to gr-484 was restored to full line pressure after incremental increases. No other transmission leaks were found. The supply to gr-483 was restored at 22:39 after v-34589 was opened and leak survey detected no leaks. Regulator station gr-483 was returned to service. The US DOT and nys psc were notified. This was a serious level incident. Note--this gas distribution incident report was generated to replace gas transmission incident report 20130011-15731.
Occurred At 2013-01-14 12:51:00
Year 2013
Report Received Date 2013-06-04 00:00:00
Iyear 2013.0
Report Number 20130073.0
Supplemental Number 15884.0
Report Type Supplemental Final
Operator Id 2704 PHMSA Enforcement
Name Consolidated Edison Co Of New York
Operator Street Address 4 Irving Place
Operator City Name New York
Operator State Abbreviation NY
Operator Postal Code 10003
Local Datetime 2013-01-13 22:28:00
Location Street Address 1060 Knollwood Road
Location City Name Town Of Greenburgh
Location County Name Westchester
Location State Abbreviation NY
Location Postal Code 10523
Location Latitude 41.070181 Google Maps OpenStreetMap
Location Longitude -73.800082 Google Maps OpenStreetMap
Nrc Rpt Datetime 2013-01-14 13:18:00
Nrc Rpt Num 1035662 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 14.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2013-01-14 12:51:00
On Site Datetime 2013-01-14 12:51:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under A Building
Depth Of Cover 28.0
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Other
System Part Details Onshore Pipeline, Including Valve Sites
Installation Year 1948.0
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Leak
Leak Type Seal Or Packing
Class Location Type Class 4 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 47993.0
Est Cost Emergency 745.0
Est Cost Other 1500.0
Est Cost Other Details Materials
Est Cost Unintentional Release 30.0
Prpty 50268.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 205.0
Normal Psig 205.0
Mop Psig 245.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Public
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak on compression coupling resulting in no pressure drop or increased flow on scada
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Pipe, Weld, Or Joint Failure
Cause Details Mechanical Joint Failure
Pwjf Failure Type Mechanical Joint Failure
Mec Fitting Involved Bolted
Mec Fitting Type Coupling
Mec Manufacturer Dresser
Mec Fitting Material Other
Mec Fitting Material Detail Materials Joined: 1st Steel, 2nd Steel
Additional Other Ind Yes
Additional Factor Details 12" Compression Coupling Seal Packing Leak
Hydrotest Conducted Ind No
Preparer Name K**** F****
Preparer Title Operations Manager-Gas Emergency Response Center
Preparer Email F*****@c****.com
Preparer Telephone 718-319-2310
Preparer Fax 718-597-5463
Authorizer Name V***** D******
Authorizer Title Department Manager-Gas Emergency Response Center
Authorizer Telephone 718-319-2350
Authorizer Email D*******@c****.com
Narrative On january 13, 2013 at 22:28 the resident at 1060 knollwood rd (tg) reported an outside odor and gas distribution services (gds) responded, investigated and detected 10% over the 12" 1948 245 psi transmission main. Gas construction -emergency response force (erf) responded and investigated, detecting 95% directly over the main. The 95% reading over the transmission main was aerated and 70% quickly returned. Contingency case 40-c-1 was identified and (2) transmission valves were initially staffed. An operational plan was developed to ensure no system impact or customer loss resulted as a result of the planned isolation of regulator stations gr-484 and gr-483. At 12:51 on january 14, 2013, transmission v-40427 was closed isolating the effected segment of transmission main. Pressure was reduced to approx 60 psi and excavation operations were initiated. Around-the-clock operations continued and additional investigation and excavation was completed. Approximately 21' south of the highest reading and initial excavation, a second excavation over a 12" compression coupling was completed and investigation continued. The coupling was found not leaking. A welded repair sleeve and (2) high hats were installed. On january 16, 2013 restoration operations were initiated at 12:39 and leak survey monitored the segment as pressure was restored in 60 psi increments and no leaks were found. The segment of isolated main was returned to normal operating condition at at 205 psi. Investigation continued and at 14:27 a visible leak on a 12" transmission coupling was confirmed at the compression end seal. An operational plan was developed and the leak was monitored around-the-clock until system conditions were favorable for isolation. There was no migration toward buildings and all subsurface structures remained gas free during this period. On january 19, 2013, the segment of main from v-40427 to gr-484 was isolated and pressure reduced. The leak was fully excavated and a welded repair sleeve was installed on the leaking coupling. The welds were tested and all tests passed. Restoration operations were initiated at 18:38, and at 21:31 the segment of main from v-40427 to gr-484 was restored to full line pressure after incremental increases. No other transmission leaks were found. The supply to gr-483 was restored at 22:39 after v-34589 was opened and leak survey detected no leaks. Regulator station gr-483 was returned to service. The US DOT and nys psc were notified. This was a serious level incident. Note--this gas distribution incident report was generated to replace gas transmission incident report 20130011-15731.

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