GD incident on 2013-04-18 — CA

Operator
Pacific Gas & Electric Co
Cause
Miscellaneous Root Causes
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$47,500
Incident datetime
2013-04-18 10:00
Report number
Location
CA, SANTA CLARA
Narrative
On april 18, 2013 a pacific gas and electric (pg&e) crew was working on an aldyl a main replacement. At approximately 1000 hours, the crew was excavating under a nearby 4-inch steel main, when the soil pushed on the pipe assembly causing a transition fitting between the adjacent 2-inch steel main and a 2-inch plastic main to become un-coupled resulting in a release of gas. The USA ticket (#063983) for the area where the main was struck is valid, and the gas facilities were properly located and marked. The backhoe operator and the utility worker involved in the incident were administered post-accident tests for drugs and alcohol. The alcohol and drug tests for both employees were returned with negative results. The pg&e investigation on the cause of the incident is ongoing. There were no injuries, no fatalities, no ignition and no media on site as a result of this incident. Out of an abundance of caution, the police department rerouted traffic on mckee road, blocked off the area, and evacuated 12 residents. The volume of gas released is less than three million cubic feet, however the cost of damages due to the release of gas is estimated to be greater than $50,000. Thus, this incident was reported to the department of transportation at 1538 hours and to the cpuc at 1550 hours when the cost of damages was estimated to exceed $50,000.
Detailed record list
Occurred At
2013-04-18 10:00:00
Year
2013
Report Received Date
2013-05-22 00:00:00
Iyear
2013.0
Report Number
20130058.0
Supplemental Number
15665.0
Report Type
Original Final
Operator Id
Name
Pacific Gas & Electric Co
Operator Street Address
6121 Bollinger Canyon Rd.
Operator City Name
San Ramon
Operator State Abbreviation
CA
Operator Postal Code
94583
Local Datetime
2013-04-18 10:00:00
Location Street Address
Mckee Road And N Claremont
Location City Name
San Jose
Location County Name
Santa Clara
Location State Abbreviation
CA
Location Postal Code
95127
Location Latitude
Location Longitude
Nrc Rpt Datetime
2013-04-18 15:38:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
820.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Incident Identified Datetime
2013-04-18 10:00:00
On Site Datetime
2013-04-18 10:00:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
75.0
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Uncased
Pipe Facility Type
Privately Owned
System Part Involved
Main
Pipe Diameter
2.0
Pipe Specification
Unknown
Pipe Manufacturer
Dupont
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Release Type
Leak
Leak Type
Crack
Class Location Type
Class 3 Location
Est Cost Oper Paid
5000.0
Est Cost Prop Damage
47500.0
Est Cost Emergency
0.0
Est Cost Other
0.0
Est Cost Unintentional Release
2500.0
Prpty
55000.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
47.0
Accident Psig
57.0
Normal Psig
57.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No scada on this part of the system
Employee Drug Test Ind
Yes
Num Employees Tested
2
Num Employees Failed
0
Contractor Drug Test Ind
Yes
Num Contractors Tested
2
Num Contractors Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Operator (First Party)
Ex Party Type
Excavation Damage By Operator (First Party)
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Utility
Excavator Equipment
Backhoe/trackhoe
Work Performed
Natural Gas
One Call Notified Ind
Yes
One Call Ticket Num
63983
One Call Center Name
Usa North
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
8.0
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Root Cause Not Listed (Comment Required)
Root Cause Type Other
Data Not Collected
Preparer Name
C***** D****
Preparer Title
Gas Compliance Engineer
Preparer Email
C***@p**.com
Preparer Telephone
925-974-4378
Preparer Fax
925-974-4232
Authorizer Name
F****** Y**
Authorizer Title
Regulatory Compliance And Support Director
Authorizer Telephone
925-974-4316
Authorizer Email
F***@p**.com
Narrative
On april 18, 2013 a pacific gas and electric (pg&e) crew was working on an aldyl a main replacement. At approximately 1000 hours, the crew was excavating under a nearby 4-inch steel main, when the soil pushed on the pipe assembly causing a transition fitting between the adjacent 2-inch steel main and a 2-inch plastic main to become un-coupled resulting in a release of gas. The USA ticket (#063983) for the area where the main was struck is valid, and the gas facilities were properly located and marked. The backhoe operator and the utility worker involved in the incident were administered post-accident tests for drugs and alcohol. The alcohol and drug tests for both employees were returned with negative results. The pg&e investigation on the cause of the incident is ongoing. There were no injuries, no fatalities, no ignition and no media on site as a result of this incident. Out of an abundance of caution, the police department rerouted traffic on mckee road, blocked off the area, and evacuated 12 residents. The volume of gas released is less than three million cubic feet, however the cost of damages due to the release of gas is estimated to be greater than $50,000. Thus, this incident was reported to the department of transportation at 1538 hours and to the cpuc at 1550 hours when the cost of damages was estimated to exceed $50,000.
Occurred At 2013-04-18 10:00:00
Year 2013
Report Received Date 2013-05-22 00:00:00
Iyear 2013.0
Report Number 20130058.0
Supplemental Number 15665.0
Report Type Original Final
Operator Id 15007 PHMSA Enforcement
Name Pacific Gas & Electric Co
Operator Street Address 6121 Bollinger Canyon Rd.
Operator City Name San Ramon
Operator State Abbreviation CA
Operator Postal Code 94583
Local Datetime 2013-04-18 10:00:00
Location Street Address Mckee Road And N Claremont
Location City Name San Jose
Location County Name Santa Clara
Location State Abbreviation CA
Location Postal Code 95127
Location Latitude 37.37821 Google Maps OpenStreetMap
Location Longitude -121.83101 Google Maps OpenStreetMap
Nrc Rpt Datetime 2013-04-18 15:38:00
Nrc Rpt Num 1044397 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 820.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Incident Identified Datetime 2013-04-18 10:00:00
On Site Datetime 2013-04-18 10:00:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 75.0
Crossing Yes
Road Crossing Ind Yes
Road Type Uncased
Pipe Facility Type Privately Owned
System Part Involved Main
Pipe Diameter 2.0
Pipe Specification Unknown
Pipe Manufacturer Dupont
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11
Release Type Leak
Leak Type Crack
Class Location Type Class 3 Location
Est Cost Oper Paid 5000.0
Est Cost Prop Damage 47500.0
Est Cost Emergency 0.0
Est Cost Other 0.0
Est Cost Unintentional Release 2500.0
Prpty 55000.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 47.0
Accident Psig 57.0
Normal Psig 57.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No scada on this part of the system
Employee Drug Test Ind Yes
Num Employees Tested 2
Num Employees Failed 0
Contractor Drug Test Ind Yes
Num Contractors Tested 2
Num Contractors Failed 0
Cause Excavation Damage
Cause Details Excavation Damage By Operator (First Party)
Ex Party Type Excavation Damage By Operator (First Party)
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype City Street
Excavator Type Utility
Excavator Equipment Backhoe/trackhoe
Work Performed Natural Gas
One Call Notified Ind Yes
One Call Ticket Num 63983
One Call Center Name Usa North
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 8.0
Root Cause Category Miscellaneous Root Causes
Root Cause Type Root Cause Not Listed (Comment Required)
Root Cause Type Other Data Not Collected
Preparer Name C***** D****
Preparer Title Gas Compliance Engineer
Preparer Email C***@p**.com
Preparer Telephone 925-974-4378
Preparer Fax 925-974-4232
Authorizer Name F****** Y**
Authorizer Title Regulatory Compliance And Support Director
Authorizer Telephone 925-974-4316
Authorizer Email F***@p**.com
Narrative On april 18, 2013 a pacific gas and electric (pg&e) crew was working on an aldyl a main replacement. At approximately 1000 hours, the crew was excavating under a nearby 4-inch steel main, when the soil pushed on the pipe assembly causing a transition fitting between the adjacent 2-inch steel main and a 2-inch plastic main to become un-coupled resulting in a release of gas. The USA ticket (#063983) for the area where the main was struck is valid, and the gas facilities were properly located and marked. The backhoe operator and the utility worker involved in the incident were administered post-accident tests for drugs and alcohol. The alcohol and drug tests for both employees were returned with negative results. The pg&e investigation on the cause of the incident is ongoing. There were no injuries, no fatalities, no ignition and no media on site as a result of this incident. Out of an abundance of caution, the police department rerouted traffic on mckee road, blocked off the area, and evacuated 12 residents. The volume of gas released is less than three million cubic feet, however the cost of damages due to the release of gas is estimated to be greater than $50,000. Thus, this incident was reported to the department of transportation at 1538 hours and to the cpuc at 1550 hours when the cost of damages was estimated to exceed $50,000.

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