GTG incident on 2013-01-26 — ND

Operator
Wbi Energy Transmission, Inc.
Cause
Excavation Issue
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,350
Incident datetime
2013-01-26 09:55
Report number
Location
ND
Narrative
A dozer that was ripping frozen ground punctured a 4" natural gas line. The line released natural gas until it was shut in and isolated. The line was properly marked by the operator, but the contractor failed to maintain distance from the pipeline while excavating. The unintentional release of gas totaled 751 mcf which does not meet the reporting threshold of 3 million cubic feet of gas, but wbi energy deemed it significant to report the incident. Natural gas service was lost to the towns of arnegard, nd and watford city, nd. Supplemental report 3/7/13 revised data in question c.3.A. From 4.5 to 4, revised data g3.6 from no to yes, and marked one-call system in g3.6.A.
Detailed record list
Report Received Date
2013-02-20 00:00:00
Iyear
2013
Report Number
20130016
Supplemental Number
15815
Report Type
Supplemental Final
Operator Id
Name
Wbi Energy Transmission, Inc.
Operator Street Address
1250 West Century Avenue
Operator City Name
Bismarck
Operator State Abbreviation
ND
Operator Postal Code
58503
Local Datetime
2013-01-26 09:50:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2013-01-26 13:51:00
Commodity Released Type
Natural Gas
Unintentional Release
751
Intentional Release
104
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-01-26 11:54:00
Restart Datetime
2013-01-26 19:05:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2013-01-26 09:55:00
On Site Datetime
2013-01-26 11:06:00
On Off Shore
Onshore
Onshore State Abbreviation
Nd
Onshore Postal Code
58831
Onshore City Name
Alexander
Onshore County Name
Mckenzie County
Designated Location
Survey Station No.
Designated Name
792+89
Pipe Fac Name
Cabin Creek - Williston
Segment Name
Watford City Lateral
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
24
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4
Pipe Wall Thickness
0.237
Pipe Smys
35000
Pipe Specification
Unknown
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1962
Manufactured Year
1962
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
4
Puncture Circum
4
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
89
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
2980
Est Cost Intentional Release
413
Est Cost Prop Damage
15350
Est Cost Emergency
1250
Est Cost Other
175000
Est Cost Other Details
The Ldc Was Involved With Restoring Service To Customers That Lost Gas Service.
Prpty
194993
Accident Psig
373
Mop Psig
752
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
55652
Internal Inspection Ind
No
Tight Mitered Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Grader/scraper
Work Performed
Grading
One Call Notified Ind
Yes
One Call Ticket Num
13004270
One Call Center Name
Ntms
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
7
Root Cause Category
Excavation Issue
Root Cause Type
Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name
K*** K***
Preparer Title
Dot Compliance Supervisor
Preparer Email
K********@w********.com
Preparer Telephone
406-359-7222
Preparer Fax
406-359-7244
Authorizer Name
K*** K***
Authorizer Title
Dot Compliance Supervisor
Authorizer Telephone
406-359-7222
Authorizer Email
K********@w********.com
Narrative
A dozer that was ripping frozen ground punctured a 4" natural gas line. The line released natural gas until it was shut in and isolated. The line was properly marked by the operator, but the contractor failed to maintain distance from the pipeline while excavating. The unintentional release of gas totaled 751 mcf which does not meet the reporting threshold of 3 million cubic feet of gas, but wbi energy deemed it significant to report the incident. Natural gas service was lost to the towns of arnegard, nd and watford city, nd. Supplemental report 3/7/13 revised data in question c.3.A. From 4.5 to 4, revised data g3.6 from no to yes, and marked one-call system in g3.6.A.
Report Received Date 2013-02-20 00:00:00
Iyear 2013
Report Number 20130016
Supplemental Number 15815
Report Type Supplemental Final
Operator Id 22655 PHMSA Enforcement
Name Wbi Energy Transmission, Inc.
Operator Street Address 1250 West Century Avenue
Operator City Name Bismarck
Operator State Abbreviation ND
Operator Postal Code 58503
Local Datetime 2013-01-26 09:50:00
Location Latitude 47.849972 Google Maps OpenStreetMap
Location Longitude -103.570833 Google Maps OpenStreetMap
Nrc Rpt Num 1036670 NRC Report How to search
Nrc Rpt Datetime 2013-01-26 13:51:00
Commodity Released Type Natural Gas
Unintentional Release 751
Intentional Release 104
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-01-26 11:54:00
Restart Datetime 2013-01-26 19:05:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2013-01-26 09:55:00
On Site Datetime 2013-01-26 11:06:00
On Off Shore Onshore
Onshore State Abbreviation Nd
Onshore Postal Code 58831
Onshore City Name Alexander
Onshore County Name Mckenzie County
Designated Location Survey Station No.
Designated Name 792+89
Pipe Fac Name Cabin Creek - Williston
Segment Name Watford City Lateral
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 24
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4
Pipe Wall Thickness 0.237
Pipe Smys 35000
Pipe Specification Unknown
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1962
Manufactured Year 1962
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 4
Puncture Circum 4
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 89
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 2980
Est Cost Intentional Release 413
Est Cost Prop Damage 15350
Est Cost Emergency 1250
Est Cost Other 175000
Est Cost Other Details The Ldc Was Involved With Restoring Service To Customers That Lost Gas Service.
Prpty 194993
Accident Psig 373
Mop Psig 752
Mop Cfr Section Not On Omb-Approved Form When Submitted View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 55652
Internal Inspection Ind No
Tight Mitered Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Grader/scraper
Work Performed Grading
One Call Notified Ind Yes
One Call Ticket Num 13004270
One Call Center Name Ntms
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 7
Root Cause Category Excavation Issue
Root Cause Type Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name K*** K***
Preparer Title Dot Compliance Supervisor
Preparer Email K********@w********.com
Preparer Telephone 406-359-7222
Preparer Fax 406-359-7244
Authorizer Name K*** K***
Authorizer Title Dot Compliance Supervisor
Authorizer Telephone 406-359-7222
Authorizer Email K********@w********.com
Narrative A dozer that was ripping frozen ground punctured a 4" natural gas line. The line released natural gas until it was shut in and isolated. The line was properly marked by the operator, but the contractor failed to maintain distance from the pipeline while excavating. The unintentional release of gas totaled 751 mcf which does not meet the reporting threshold of 3 million cubic feet of gas, but wbi energy deemed it significant to report the incident. Natural gas service was lost to the towns of arnegard, nd and watford city, nd. Supplemental report 3/7/13 revised data in question c.3.A. From 4.5 to 4, revised data g3.6 from no to yes, and marked one-call system in g3.6.A.

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