GD incident on 2012-12-21 — NJ

Operator
South Jersey Gas Co
Cause
Natural Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2012-12-21 00:10
Report number
Location
NJ, CAMDEN
Narrative
A tree root cracked the plastic service tee serving 36 w. Brookline drive. The cracked plastic service tee and attached piping was sent to an independent testing laboratory for analysis.
Detailed record list
Occurred At
2012-12-21 00:10:00
Year
2012
Report Received Date
2013-01-14 00:00:00
Iyear
2012.0
Report Number
20130005.0
Supplemental Number
15581.0
Report Type
Original
Operator Id
Name
South Jersey Gas Co
Operator Street Address
101 South Lincoln Place
Operator City Name
Atlantic City
Operator State Abbreviation
NJ
Operator Postal Code
08401
Local Datetime
2012-12-21 00:10:00
Location Street Address
35 W. Brookline Drive
Location City Name
Laurel Springs
Location County Name
Camden
Location State Abbreviation
NJ
Location Postal Code
08021
Location Latitude
Location Longitude
Nrc Rpt Datetime
2012-12-21 11:44:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
100.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
Yes
Num Pub Evacuated
15.0
Incident Identified Datetime
2012-12-21 00:10:00
On Site Datetime
2012-12-21 00:33:00
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Service
Installation Year
1985.0
Pipe Diameter
0.75
Pipe Specification
Astm D2513
Pipe Manufacturer
Dupont
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Material Pe Pipe Code
2306
Release Type
Leak
Leak Type
Crack
Class Location Type
Class 3 Location
Est Cost Oper Paid
233600.0
Est Cost Prop Damage
5000.0
Est Cost Emergency
81000.0
Est Cost Other
0.0
Est Cost Unintentional Release
1000.0
Prpty
320600.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
8.0
Accident Psig
60.0
Normal Psig
60.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Other Natural Force Damage
Natural Force Type
Other Natural Force Damage
Nf Other Details
Tree Root Cracked Plastic Service Tee Piece
Nf Extreme Weather Ind
No
Preparer Name
D**** N*****
Preparer Title
Manager Compliance And Quality Assurance
Preparer Email
D******@s***********.com
Preparer Telephone
609-561-9000
Preparer Fax
609-704-1802
Authorizer Name
D**** N*****
Authorizer Title
Manager Compliance And Quality Assurance
Authorizer Telephone
609-561-9000
Authorizer Email
D******@s***********.com
Narrative
A tree root cracked the plastic service tee serving 36 w. Brookline drive. The cracked plastic service tee and attached piping was sent to an independent testing laboratory for analysis.
Occurred At 2012-12-21 00:10:00
Year 2012
Report Received Date 2013-01-14 00:00:00
Iyear 2012.0
Report Number 20130005.0
Supplemental Number 15581.0
Report Type Original
Operator Id 18440 PHMSA Enforcement
Name South Jersey Gas Co
Operator Street Address 101 South Lincoln Place
Operator City Name Atlantic City
Operator State Abbreviation NJ
Operator Postal Code 08401
Local Datetime 2012-12-21 00:10:00
Location Street Address 35 W. Brookline Drive
Location City Name Laurel Springs
Location County Name Camden
Location State Abbreviation NJ
Location Postal Code 08021
Location Latitude 39.823959 Google Maps OpenStreetMap
Location Longitude -75.052967 Google Maps OpenStreetMap
Nrc Rpt Datetime 2012-12-21 11:44:00
Nrc Rpt Num 1033908 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 100.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind Yes
Num Pub Evacuated 15.0
Incident Identified Datetime 2012-12-21 00:10:00
On Site Datetime 2012-12-21 00:33:00
Federal No
Location Type Private Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Service
Installation Year 1985.0
Pipe Diameter 0.75
Pipe Specification Astm D2513
Pipe Manufacturer Dupont
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11
Material Pe Pipe Code 2306
Release Type Leak
Leak Type Crack
Class Location Type Class 3 Location
Est Cost Oper Paid 233600.0
Est Cost Prop Damage 5000.0
Est Cost Emergency 81000.0
Est Cost Other 0.0
Est Cost Unintentional Release 1000.0
Prpty 320600.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 8.0
Accident Psig 60.0
Normal Psig 60.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Other Natural Force Damage
Natural Force Type Other Natural Force Damage
Nf Other Details Tree Root Cracked Plastic Service Tee Piece
Nf Extreme Weather Ind No
Preparer Name D**** N*****
Preparer Title Manager Compliance And Quality Assurance
Preparer Email D******@s***********.com
Preparer Telephone 609-561-9000
Preparer Fax 609-704-1802
Authorizer Name D**** N*****
Authorizer Title Manager Compliance And Quality Assurance
Authorizer Telephone 609-561-9000
Authorizer Email D******@s***********.com
Narrative A tree root cracked the plastic service tee serving 36 w. Brookline drive. The cracked plastic service tee and attached piping was sent to an independent testing laboratory for analysis.

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