HL incident on 2012-12-01 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$7,000
Incident datetime
2012-12-01 20:44
Report number
Location
TX
Narrative
At 20:44 cst pipeline control received fire detection, then a hazardous gas alarm remotely. At 21:20 cst a local area technician arrived and confirmed a small flash fire had occurred on forsan station, turbine #4 operating on the seminole red mainline (lid 50). The fire was out prior to the technician's arrival. There was minor damage to horizontal pump wiring and conduits. Investigation of the accident determined the loss of inboard and outboard pump seals resulted in the release of natural gasoline which ignited due to the high temperature of the gas turbine driver. The loss of seal integrity was due to a reduction in seal flush flow due to build-up of sediments from the pipeline.
Detailed record list
Report Received Date
2012-12-28 00:00:00
Iyear
2012
Report Number
20120375
Supplemental Number
17598
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-12-01 20:44:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.1
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2012-12-01 20:44:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-12-01 20:44:00
Restart Datetime
2012-12-02 00:17:00
On Site Datetime
2012-12-01 21:20:00
Nrc Rpt Datetime
2012-12-01 22:40:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Forsan Station
Segment Name
Seminole Red Lid 50
Onshore State Abbreviation
Tx
Onshore Postal Code
79720
Onshore City Name
Forsan
Onshore County Name
Howard
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
7000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
7000
Accident Psig
395
Mop Psig
1330
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller received the haz gas and seal fail alarms and called a technician to investigate. There was no other information from scada indications to mandate further actions.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
Reduction In Seal Flush Flow Due To Build-Up Of Sediments From The Pipeline.
Preparer Name
N*** T*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
N*******@e****.com
Preparer Telephone
7133812493
Prepared Date
2013-03-19 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
7133812493
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
N*******@e****.com
Narrative
At 20:44 cst pipeline control received fire detection, then a hazardous gas alarm remotely. At 21:20 cst a local area technician arrived and confirmed a small flash fire had occurred on forsan station, turbine #4 operating on the seminole red mainline (lid 50). The fire was out prior to the technician's arrival. There was minor damage to horizontal pump wiring and conduits. Investigation of the accident determined the loss of inboard and outboard pump seals resulted in the release of natural gasoline which ignited due to the high temperature of the gas turbine driver. The loss of seal integrity was due to a reduction in seal flush flow due to build-up of sediments from the pipeline.
Report Received Date 2012-12-28 00:00:00
Iyear 2012
Report Number 20120375
Supplemental Number 17598
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2012-12-01 20:44:00
Location Latitude 32.113857 Google Maps OpenStreetMap
Location Longitude -101.255144 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.1
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2012-12-01 20:44:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-12-01 20:44:00
Restart Datetime 2012-12-02 00:17:00
On Site Datetime 2012-12-01 21:20:00
Nrc Rpt Datetime 2012-12-01 22:40:00
Nrc Rpt Num 1032064 NRC Report How to search
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Forsan Station
Segment Name Seminole Red Lid 50
Onshore State Abbreviation Tx
Onshore Postal Code 79720
Onshore City Name Forsan
Onshore County Name Howard
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 7000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 7000
Accident Psig 395
Mop Psig 1330
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller received the haz gas and seal fail alarms and called a technician to investigate. There was no other information from scada indications to mandate further actions.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details Reduction In Seal Flush Flow Due To Build-Up Of Sediments From The Pipeline.
Preparer Name N*** T*****
Preparer Title Pipeline Compliance Engineer
Preparer Email N*******@e****.com
Preparer Telephone 7133812493
Prepared Date 2013-03-19 00:00:00
Authorizer Name N*** T*****
Authorizer Telephone 7133812493
Authorizer Title Pipeline Compliance Engineer
Authorizer Email N*******@e****.com
Narrative At 20:44 cst pipeline control received fire detection, then a hazardous gas alarm remotely. At 21:20 cst a local area technician arrived and confirmed a small flash fire had occurred on forsan station, turbine #4 operating on the seminole red mainline (lid 50). The fire was out prior to the technician's arrival. There was minor damage to horizontal pump wiring and conduits. Investigation of the accident determined the loss of inboard and outboard pump seals resulted in the release of natural gasoline which ignited due to the high temperature of the gas turbine driver. The loss of seal integrity was due to a reduction in seal flush flow due to build-up of sediments from the pipeline.

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