HL incident on 2012-11-21 — KS

Operator
Nustar Pipeline Operating Partnership L.p.
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$26,000
Incident datetime
2012-11-21 13:30
Report number
Location
KS
Narrative
Landowner notified nustar geneva terminal in person that pipeline may have a leak. Terminal personnel responded and confirmed a leak at 13:30 on 11/21/2012. The cut out section of pipe has been sent to keifner for metallurgical analysis. A supplemental report will be filed upon receiving results. Soils were excavated as the form of remediation. 5400 cubic yards of soil was approved by ndeq to be landfarmed on site. 2300 cubic yards of soil was hauled to a local permitted landfill. Site remediation is complete as of this report. Metallurgical analysis result - the cause of the leak was pressure cycle induced fatigue cracking that initiated at a pre-existing hook crack in the electric-resistance weld (erw) seam. The original hook crack was open to the external pipe surface and measured 8.49 inches long by 0.5 inch deep (equivalent to 27% of the normal wall thickness). A portion of this hook crack enlarged due to pressure cycle induced fatigue, resulting in a leak opening measured 2.0 inches long on the internal pipe surface.
Detailed record list
Report Received Date
2012-12-21 00:00:00
Iyear
2012
Report Number
20120374
Supplemental Number
17670
Report Type
Supplemental Final
Operator Id
Name
Nustar Pipeline Operating Partnership L.p.
Operator Street Address
7340 W. 21st Street N, Suite 200
Operator City Name
Wichita
Operator State Abbreviation
KS
Operator Postal Code
67205
Local Datetime
2012-11-21 13:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
60
Intentional Release Bbls
0
Recovered Bbls
60
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2012-11-21 13:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-11-21 13:30:00
Restart Datetime
2012-11-22 20:00:00
On Site Datetime
2012-11-21 14:30:00
Nrc Rpt Datetime
2012-11-21 15:03:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Geneva To Norfolk 8 Inch
Segment Name
Geneva - 8 Inch To York
Onshore State Abbreviation
Ne
Onshore Postal Code
68354
Onshore City Name
Fairmont
Onshore County Name
Fillmore
Designated Location
Milepost/valve Station
Designated Name
Mp 5.93
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
84
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.188
Pipe Smys
42000
Pipe Specification
Api 5l-X42
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Stupp Corporation
Pipe Coating Type
Cold Applied Tape
Installation Year
1965
Manufactured Year
1965
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Leak Type Other
Metallurgical Analysis
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
3.5
Rel Water Name
Man-Made Surface Pond Used For Irrigation.
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
15000
Est Cost Gas Released
7500
Est Cost Prop Damage
26000
Est Cost Emergency
260000
Est Cost Environmental
624500
Est Cost Other
0
Prpty
933000
Accident Psig
975
Mop Psig
1205
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
Yes
Exceed Restriction Ind
No
Phmsa Restriction Ind
Not Mandated
Length Segment Isolated
73920
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
Yes
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Fatigue Vibr Related
Yes
Failure Subtype
Pressure-Related
Additional Crack Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Emat Ind
Yes
Axial Recent Year
2011
Geometry Recent Year
2011
Emat Recent Year
2011
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1994
Hydrtst Most Rcnt Pressure
1601
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
D***** J* T******
Preparer Title
Director - Hse
Preparer Email
D**********@n***********.com
Preparer Telephone
316-721-7056
Preparer Fax
316-773-9001
Prepared Date
2013-03-25 00:00:00
Authorizer Name
G***** K*********
Authorizer Telephone
316-721-7052
Authorizer Title
Vp Gm
Authorizer Email
G**************@n***********.com
Narrative
Landowner notified nustar geneva terminal in person that pipeline may have a leak. Terminal personnel responded and confirmed a leak at 13:30 on 11/21/2012. The cut out section of pipe has been sent to keifner for metallurgical analysis. A supplemental report will be filed upon receiving results. Soils were excavated as the form of remediation. 5400 cubic yards of soil was approved by ndeq to be landfarmed on site. 2300 cubic yards of soil was hauled to a local permitted landfill. Site remediation is complete as of this report. Metallurgical analysis result - the cause of the leak was pressure cycle induced fatigue cracking that initiated at a pre-existing hook crack in the electric-resistance weld (erw) seam. The original hook crack was open to the external pipe surface and measured 8.49 inches long by 0.5 inch deep (equivalent to 27% of the normal wall thickness). A portion of this hook crack enlarged due to pressure cycle induced fatigue, resulting in a leak opening measured 2.0 inches long on the internal pipe surface.
Report Received Date 2012-12-21 00:00:00
Iyear 2012
Report Number 20120374
Supplemental Number 17670
Report Type Supplemental Final
Operator Id 10012 PHMSA Enforcement
Name Nustar Pipeline Operating Partnership L.p.
Operator Street Address 7340 W. 21st Street N, Suite 200
Operator City Name Wichita
Operator State Abbreviation KS
Operator Postal Code 67205
Local Datetime 2012-11-21 13:30:00
Location Latitude 40.621988 Google Maps OpenStreetMap
Location Longitude -97.549726 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 60
Intentional Release Bbls 0
Recovered Bbls 60
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2012-11-21 13:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-11-21 13:30:00
Restart Datetime 2012-11-22 20:00:00
On Site Datetime 2012-11-21 14:30:00
Nrc Rpt Datetime 2012-11-21 15:03:00
Nrc Rpt Num 1031281 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Geneva To Norfolk 8 Inch
Segment Name Geneva - 8 Inch To York
Onshore State Abbreviation Ne
Onshore Postal Code 68354
Onshore City Name Fairmont
Onshore County Name Fillmore
Designated Location Milepost/valve Station
Designated Name Mp 5.93
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 84
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.188
Pipe Smys 42000
Pipe Specification Api 5l-X42
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Stupp Corporation
Pipe Coating Type Cold Applied Tape
Installation Year 1965
Manufactured Year 1965
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Leak Type Other Metallurgical Analysis
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 3.5
Rel Water Name Man-Made Surface Pond Used For Irrigation.
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 15000
Est Cost Gas Released 7500
Est Cost Prop Damage 26000
Est Cost Emergency 260000
Est Cost Environmental 624500
Est Cost Other 0
Prpty 933000
Accident Psig 975
Mop Psig 1205
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind Yes
Exceed Restriction Ind No
Phmsa Restriction Ind Not Mandated
Length Segment Isolated 73920
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind Yes
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Fatigue Vibr Related Yes
Failure Subtype Pressure-Related
Additional Crack Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Emat Ind Yes
Axial Recent Year 2011
Geometry Recent Year 2011
Emat Recent Year 2011
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1994
Hydrtst Most Rcnt Pressure 1601
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name D***** J* T******
Preparer Title Director - Hse
Preparer Email D**********@n***********.com
Preparer Telephone 316-721-7056
Preparer Fax 316-773-9001
Prepared Date 2013-03-25 00:00:00
Authorizer Name G***** K*********
Authorizer Telephone 316-721-7052
Authorizer Title Vp Gm
Authorizer Email G**************@n***********.com
Narrative Landowner notified nustar geneva terminal in person that pipeline may have a leak. Terminal personnel responded and confirmed a leak at 13:30 on 11/21/2012. The cut out section of pipe has been sent to keifner for metallurgical analysis. A supplemental report will be filed upon receiving results. Soils were excavated as the form of remediation. 5400 cubic yards of soil was approved by ndeq to be landfarmed on site. 2300 cubic yards of soil was hauled to a local permitted landfill. Site remediation is complete as of this report. Metallurgical analysis result - the cause of the leak was pressure cycle induced fatigue cracking that initiated at a pre-existing hook crack in the electric-resistance weld (erw) seam. The original hook crack was open to the external pipe surface and measured 8.49 inches long by 0.5 inch deep (equivalent to 27% of the normal wall thickness). A portion of this hook crack enlarged due to pressure cycle induced fatigue, resulting in a leak opening measured 2.0 inches long on the internal pipe surface.

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