Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2012-11-26 — OK
Operator
Bkep Crude, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$498
Incident datetime
2012-11-26 10:00
Report number
Location
OK
Narrative
A seal on a mixer on breakout storage tank 2518 in the bkep crude, llc north tankfarm in cushing, ok occurred on 11/26/2012. Approximately 2 bbls of crude oil leaked onto the ground. The oil was cleaned up promptly and the mixer was repaired.
Detailed record list
Report Received Date
2012-12-19 00:00:00
Iyear
2012
Report Number
20120362
Supplemental Number
19604
Report Type
Supplemental Final
Operator Id
32481
Name
Bkep Crude, Llc
Operator Street Address
6060 American Plaza Suite 600
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74135
Local Datetime
2012-11-26 10:00:00
Location Latitude
36.0191
Location Longitude
-96.7569
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-11-26 10:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Occurred On Tank Mixer
On Site Datetime
2012-11-26 10:05:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing North Tankfarm
Segment Name
Tank 2518
Onshore State Abbreviation
Ok
Onshore Postal Code
74032
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Survey Station No.
Designated Name
Cushing North
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Pipe Facility Type
Intrastate
Item Involved
Other
Tank Type
Atmospheric
Item Involved Details
Mixer Seal On Tank 2518
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
160
Est Cost Prop Damage
498
Est Cost Emergency
1758
Est Cost Environmental
0
Est Cost Other
0
Prpty
2416
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Preparer Name
R***** S*****
Preparer Title
Mgr. Env And Dot Pipeline
Preparer Email
R******@b***.com
Preparer Telephone
5129040788
Preparer Fax
9182374001
Prepared Date
2014-07-28 00:00:00
Authorizer Name
R***** S*****
Authorizer Telephone
5129040788
Authorizer Title
Mgr. Env And Dot Pipeline
Authorizer Email
R******@b***.com
Narrative
A seal on a mixer on breakout storage tank 2518 in the bkep crude, llc north tankfarm in cushing, ok occurred on 11/26/2012. Approximately 2 bbls of crude oil leaked onto the ground. The oil was cleaned up promptly and the mixer was repaired.
| Report Received Date | 2012-12-19 00:00:00 |
|---|---|
| Iyear | 2012 |
| Report Number | 20120362 |
| Supplemental Number | 19604 |
| Report Type | Supplemental Final |
| Operator Id | 32481 PHMSA Enforcement |
| Name | Bkep Crude, Llc |
| Operator Street Address | 6060 American Plaza Suite 600 |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74135 |
| Local Datetime | 2012-11-26 10:00:00 |
| Location Latitude | 36.0191 Google Maps OpenStreetMap |
| Location Longitude | -96.7569 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 2 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2012-11-26 10:00:00 |
| System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Leak Occurred On Tank Mixer |
| On Site Datetime | 2012-11-26 10:05:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Cushing North Tankfarm |
| Segment Name | Tank 2518 |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 74032 |
| Onshore City Name | Cushing |
| Onshore County Name | Payne |
| Designated Location | Survey Station No. |
| Designated Name | Cushing North |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Tank, Including Attached Appurtenances |
| Pipe Facility Type | Intrastate |
| Item Involved | Other |
| Tank Type | Atmospheric |
| Item Involved Details | Mixer Seal On Tank 2518 |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 160 |
| Est Cost Prop Damage | 498 |
| Est Cost Emergency | 1758 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 2416 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Other Equipment Failure |
| Eq Failure Type | Other Equipment Failure |
| Preparer Name | R***** S***** |
| Preparer Title | Mgr. Env And Dot Pipeline |
| Preparer Email | R******@b***.com |
| Preparer Telephone | 5129040788 |
| Preparer Fax | 9182374001 |
| Prepared Date | 2014-07-28 00:00:00 |
| Authorizer Name | R***** S***** |
| Authorizer Telephone | 5129040788 |
| Authorizer Title | Mgr. Env And Dot Pipeline |
| Authorizer Email | R******@b***.com |
| Narrative | A seal on a mixer on breakout storage tank 2518 in the bkep crude, llc north tankfarm in cushing, ok occurred on 11/26/2012. Approximately 2 bbls of crude oil leaked onto the ground. The oil was cleaned up promptly and the mixer was repaired. |
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