HL incident on 2012-12-05 — TX

Operator
Shell Pipeline Co., L.p.
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,000
Incident datetime
2012-12-05 17:00
Report number
Location
TX
Narrative
Insulating gasket on the downstream side of a mainline block valve at iowa pump station began leaking following the connection of a bypass line just downstream of the block valve. The leak was first noticed as small enough to tighten the flange studs and nuts which stopped the release for over one hour. The release began again. The pipeline was segmented by closing other mainline block valve which isolated a 7 mile long segment of pipeline while ethylene pipeline was shut down. The isolated segment was blown down through several flares. The flange gasket continued to leak until the pressure dropped to approx. 550 psi. At which time it stopped. The isolated pipeline segment continued to be blown down until it was safe to remove and replace the gasket. The gasket was replaced on 12/8 and restarted on 12/9. The gasket was a micarta insulating gasket used to isolate the pipeline segments. This type of insulating gasket was commonly utilized. It was found to be in good condition. An investigation determined the cause of the release was due to the loss of support of the aboveground flange set while connecting the temporary bypass piping downstream of the flange set. 3/13/2013 - verified e5f per request from PHMSA. 11/12/13 - spoke with blaine keener, PHMSA - requested the recovered volume be removed for the amount of the intentional volume.
Detailed record list
Report Received Date
2012-12-13 00:00:00
Iyear
2012
Report Number
20120359
Supplemental Number
18718
Report Type
Supplemental Final
Operator Id
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2012-12-05 17:00:00
Location Latitude
Location Longitude
-93.04560277
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethylene
Unintentional Release Bbls
329
Intentional Release Bbls
4925
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2012-12-05 17:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-12-05 17:00:00
Restart Datetime
2012-12-09 07:30:00
On Site Datetime
2012-12-05 17:00:00
Nrc Rpt Datetime
2012-12-05 17:47:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Iowa Pump Station Ml Bv
Onshore State Abbreviation
La
Onshore Postal Code
70647
Onshore City Name
Iowa
Onshore County Name
Calcasieu
Designated Location
Milepost/valve Station
Designated Name
121
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
1990
Material Involved
Material Other Than Carbon Steel
Material Details
Insulating Gasket
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
218500
Est Cost Prop Damage
25000
Est Cost Emergency
250000
Est Cost Environmental
0
Est Cost Other
0
Prpty
493500
Accident Psig
1163
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
36960
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was immediately identified by field personnel and the system was shut down in a safe and efficient manner.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Support Ind
Yes
Preparer Name
R****** K*****
Preparer Title
Regulatory Specialist
Preparer Email
R*************@s****.com
Preparer Telephone
7132411064
Prepared Date
2013-11-12 00:00:00
Authorizer Name
B**** S*******
Authorizer Telephone
7132413620
Authorizer Title
Integrity And Regulatory Services Manager
Authorizer Email
B*************@s****.com
Narrative
Insulating gasket on the downstream side of a mainline block valve at iowa pump station began leaking following the connection of a bypass line just downstream of the block valve. The leak was first noticed as small enough to tighten the flange studs and nuts which stopped the release for over one hour. The release began again. The pipeline was segmented by closing other mainline block valve which isolated a 7 mile long segment of pipeline while ethylene pipeline was shut down. The isolated segment was blown down through several flares. The flange gasket continued to leak until the pressure dropped to approx. 550 psi. At which time it stopped. The isolated pipeline segment continued to be blown down until it was safe to remove and replace the gasket. The gasket was replaced on 12/8 and restarted on 12/9. The gasket was a micarta insulating gasket used to isolate the pipeline segments. This type of insulating gasket was commonly utilized. It was found to be in good condition. An investigation determined the cause of the release was due to the loss of support of the aboveground flange set while connecting the temporary bypass piping downstream of the flange set. 3/13/2013 - verified e5f per request from PHMSA. 11/12/13 - spoke with blaine keener, PHMSA - requested the recovered volume be removed for the amount of the intentional volume.
Report Received Date 2012-12-13 00:00:00
Iyear 2012
Report Number 20120359
Supplemental Number 18718
Report Type Supplemental Final
Operator Id 31174 PHMSA Enforcement
Name Shell Pipeline Co., L.p.
Operator Street Address 150 North Dairy Ashford Road Wck Bldg. A
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2012-12-05 17:00:00
Location Latitude 30.15735228 Google Maps OpenStreetMap
Location Longitude -93.04560277 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethylene
Unintentional Release Bbls 329
Intentional Release Bbls 4925
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2012-12-05 17:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-12-05 17:00:00
Restart Datetime 2012-12-09 07:30:00
On Site Datetime 2012-12-05 17:00:00
Nrc Rpt Datetime 2012-12-05 17:47:00
Nrc Rpt Num 1032428 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Iowa Pump Station Ml Bv
Onshore State Abbreviation La
Onshore Postal Code 70647
Onshore City Name Iowa
Onshore County Name Calcasieu
Designated Location Milepost/valve Station
Designated Name 121
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 1990
Material Involved Material Other Than Carbon Steel
Material Details Insulating Gasket
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 218500
Est Cost Prop Damage 25000
Est Cost Emergency 250000
Est Cost Environmental 0
Est Cost Other 0
Prpty 493500
Accident Psig 1163
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 36960
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was immediately identified by field personnel and the system was shut down in a safe and efficient manner.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Support Ind Yes
Preparer Name R****** K*****
Preparer Title Regulatory Specialist
Preparer Email R*************@s****.com
Preparer Telephone 7132411064
Prepared Date 2013-11-12 00:00:00
Authorizer Name B**** S*******
Authorizer Telephone 7132413620
Authorizer Title Integrity And Regulatory Services Manager
Authorizer Email B*************@s****.com
Narrative Insulating gasket on the downstream side of a mainline block valve at iowa pump station began leaking following the connection of a bypass line just downstream of the block valve. The leak was first noticed as small enough to tighten the flange studs and nuts which stopped the release for over one hour. The release began again. The pipeline was segmented by closing other mainline block valve which isolated a 7 mile long segment of pipeline while ethylene pipeline was shut down. The isolated segment was blown down through several flares. The flange gasket continued to leak until the pressure dropped to approx. 550 psi. At which time it stopped. The isolated pipeline segment continued to be blown down until it was safe to remove and replace the gasket. The gasket was replaced on 12/8 and restarted on 12/9. The gasket was a micarta insulating gasket used to isolate the pipeline segments. This type of insulating gasket was commonly utilized. It was found to be in good condition. An investigation determined the cause of the release was due to the loss of support of the aboveground flange set while connecting the temporary bypass piping downstream of the flange set. 3/13/2013 - verified e5f per request from PHMSA. 11/12/13 - spoke with blaine keener, PHMSA - requested the recovered volume be removed for the amount of the intentional volume.

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