HL incident on 2012-11-09 — KS

Operator
Koch Pipeline Company, L.p.
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2012-11-09 00:48
Report number
Location
KS
Narrative
On november 9, 2012 at 00:48, the kpl control center received a seal leak alarm at the san antonio pump station. A kpl operation technician arrived onsite at 01:22, observed the unit 2 inboard seal displaced; with product leaking. At 01:45, kpl's control center shutdown pump unit 3 and to isolate the pump station, closed valves 13 and 14. Valve 44 was opened to make adjustments to pipeline flow. The leak was stopped by blowing down the case pressure line and depressurizing the system. Additional kpl field resources were notified and began containment and clean up. Kpl osro, tas environmental services arrived at 04:00 and began removal of the product inside the pump base utilizing a vacuum truck. Kpl contractor, sexton inc., arrived at 09:00 and removed contaminated soil and rock from around the skid area. The investigation revealed that the unit 2 inboard seal failure contributed to the estimated 2 barrels of gasoline released from the system. The line was started up using additional pumps, already installed and the pumping equipment was been removed and sent for repair.
Detailed record list
Report Received Date
2012-12-07 00:00:00
Iyear
2012
Report Number
20120352
Supplemental Number
18181
Report Type
Supplemental Final
Operator Id
Name
Koch Pipeline Company, L.p.
Operator Street Address
4111 East 37th Street North
Operator City Name
Wichita
Operator State Abbreviation
KS
Operator Postal Code
67220
Local Datetime
2012-11-09 00:48:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
2
Intentional Release Bbls
0
Recovered Bbls
1.95
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2012-11-09 00:48:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-11-09 01:45:00
Restart Datetime
2012-11-09 18:07:00
On Site Datetime
2012-11-09 01:22:00
Nrc Rpt Datetime
2012-11-09 02:27:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
San Antonio Pump Station
Segment Name
San Antonio Pump Station-6013
Onshore State Abbreviation
Tx
Onshore Postal Code
78219
Onshore City Name
San Antonio
Onshore County Name
Bexar
Designated Location
Milepost/valve Station
Designated Name
6013
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
260
Est Cost Prop Damage
0
Est Cost Emergency
3102
Est Cost Environmental
52422
Est Cost Other
0
Prpty
55784
Accident Psig
1623
Mop Psig
2160
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The system was operating as designed, since pump 2 is automatically isolated & locked out (due to a seal leak alarm) until additional field resources arrive onsite to investigate &/or clear alarms. Upon receipt of the seal leak alarm, the controller started pump unit 3.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
2
Num Employees Failed
0
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
The Seal Failed At Less Pressure That It Was Designed/rated For.
Preparer Name
C**** K*******
Preparer Title
Program Coordinator
Preparer Email
C*************@k***********.com
Preparer Telephone
316-828-4121
Preparer Fax
316-529-6377
Prepared Date
2013-06-11 00:00:00
Authorizer Name
C**** K*******
Authorizer Telephone
316-828-4121
Authorizer Title
Program Coordinator
Authorizer Email
C*************@k***********.com
Narrative
On november 9, 2012 at 00:48, the kpl control center received a seal leak alarm at the san antonio pump station. A kpl operation technician arrived onsite at 01:22, observed the unit 2 inboard seal displaced; with product leaking. At 01:45, kpl's control center shutdown pump unit 3 and to isolate the pump station, closed valves 13 and 14. Valve 44 was opened to make adjustments to pipeline flow. The leak was stopped by blowing down the case pressure line and depressurizing the system. Additional kpl field resources were notified and began containment and clean up. Kpl osro, tas environmental services arrived at 04:00 and began removal of the product inside the pump base utilizing a vacuum truck. Kpl contractor, sexton inc., arrived at 09:00 and removed contaminated soil and rock from around the skid area. The investigation revealed that the unit 2 inboard seal failure contributed to the estimated 2 barrels of gasoline released from the system. The line was started up using additional pumps, already installed and the pumping equipment was been removed and sent for repair.
Report Received Date 2012-12-07 00:00:00
Iyear 2012
Report Number 20120352
Supplemental Number 18181
Report Type Supplemental Final
Operator Id 22855 PHMSA Enforcement
Name Koch Pipeline Company, L.p.
Operator Street Address 4111 East 37th Street North
Operator City Name Wichita
Operator State Abbreviation KS
Operator Postal Code 67220
Local Datetime 2012-11-09 00:48:00
Location Latitude 29.11242 Google Maps OpenStreetMap
Location Longitude -98.11987 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 2
Intentional Release Bbls 0
Recovered Bbls 1.95
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2012-11-09 00:48:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-11-09 01:45:00
Restart Datetime 2012-11-09 18:07:00
On Site Datetime 2012-11-09 01:22:00
Nrc Rpt Datetime 2012-11-09 02:27:00
Nrc Rpt Num 1030103 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name San Antonio Pump Station
Segment Name San Antonio Pump Station-6013
Onshore State Abbreviation Tx
Onshore Postal Code 78219
Onshore City Name San Antonio
Onshore County Name Bexar
Designated Location Milepost/valve Station
Designated Name 6013
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 260
Est Cost Prop Damage 0
Est Cost Emergency 3102
Est Cost Environmental 52422
Est Cost Other 0
Prpty 55784
Accident Psig 1623
Mop Psig 2160
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The system was operating as designed, since pump 2 is automatically isolated & locked out (due to a seal leak alarm) until additional field resources arrive onsite to investigate &/or clear alarms. Upon receipt of the seal leak alarm, the controller started pump unit 3.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 2
Num Employees Failed 0
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details The Seal Failed At Less Pressure That It Was Designed/rated For.
Preparer Name C**** K*******
Preparer Title Program Coordinator
Preparer Email C*************@k***********.com
Preparer Telephone 316-828-4121
Preparer Fax 316-529-6377
Prepared Date 2013-06-11 00:00:00
Authorizer Name C**** K*******
Authorizer Telephone 316-828-4121
Authorizer Title Program Coordinator
Authorizer Email C*************@k***********.com
Narrative On november 9, 2012 at 00:48, the kpl control center received a seal leak alarm at the san antonio pump station. A kpl operation technician arrived onsite at 01:22, observed the unit 2 inboard seal displaced; with product leaking. At 01:45, kpl's control center shutdown pump unit 3 and to isolate the pump station, closed valves 13 and 14. Valve 44 was opened to make adjustments to pipeline flow. The leak was stopped by blowing down the case pressure line and depressurizing the system. Additional kpl field resources were notified and began containment and clean up. Kpl osro, tas environmental services arrived at 04:00 and began removal of the product inside the pump base utilizing a vacuum truck. Kpl contractor, sexton inc., arrived at 09:00 and removed contaminated soil and rock from around the skid area. The investigation revealed that the unit 2 inboard seal failure contributed to the estimated 2 barrels of gasoline released from the system. The line was started up using additional pumps, already installed and the pumping equipment was been removed and sent for repair.

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