HL incident on 2012-11-23 — WY

Operator
Suncor Energy (Usa) Pipeline Co.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2012-11-23 10:30
Report number
Location
WY
Narrative
Local station operator was making a daily tour of the station and found oil coming up from the ground. He then called the control center to shut down the blend and start pumping out of another tank. He then contacted a contractor with a vacuum truck to pick up oil. Then he contacted a dirt contractor to come and dig up location of the spill to find the source of the oil. Pipe was removed and blinded off. Pipe has been sent in to a lab for future analysis. The pipe that was involved in the accident was a prover line that went 3 foot below ground. Suncor believes that this was a point for water dropout and the pipe has internal corrsion from the water drop out.
Detailed record list
Report Received Date
2012-12-06 00:00:00
Iyear
2012
Report Number
20120351
Supplemental Number
18433
Report Type
Supplemental Final
Operator Id
Name
Suncor Energy (Usa) Pipeline Co.
Operator Street Address
1700 Cutler Rd.
Operator City Name
Cheyenne
Operator State Abbreviation
WY
Operator Postal Code
82001
Local Datetime
2012-11-23 10:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
20
Recovered Bbls
15
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2012-11-23 10:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Leak On Blend Pump Prover Line; Contained In Tank 1 Dike
On Site Datetime
2012-11-23 10:40:00
Nrc Rpt Datetime
2012-11-26 10:00:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Guernsey Pump Station
Segment Name
Cennenial / 3965
Onshore State Abbreviation
Wy
Onshore Postal Code
82214
Onshore City Name
Guernsey
Onshore County Name
Platte
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4.5
Pipe Wall Thickness
0.237
Pipe Smys
42000
Pipe Specification
Api 5l-X42
Pipe Seam Type
Seamless
Pipe Manufacturer
United States Steel
Pipe Coating Type
Extruded Polyehylene
Installation Year
2004
Manufactured Year
2004
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
5000
Est Cost Emergency
0
Est Cost Environmental
10000
Est Cost Other
0
Prpty
15500
Accident Psig
180
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pipe was upstream of mainline leak detection system. No abnormal operating conditions were involved.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
L**** H******
Preparer Title
Manager- Regulatory Complaince- Row - Training
Preparer Email
L*******@s*****.com
Preparer Telephone
3077758101
Preparer Fax
3076376633
Prepared Date
2013-08-09 00:00:00
Authorizer Name
L**** H******
Authorizer Telephone
3077758101
Authorizer Title
Manager- Regulatory Complaince- Row - Training
Authorizer Email
L*******@s*****.com
Narrative
Local station operator was making a daily tour of the station and found oil coming up from the ground. He then called the control center to shut down the blend and start pumping out of another tank. He then contacted a contractor with a vacuum truck to pick up oil. Then he contacted a dirt contractor to come and dig up location of the spill to find the source of the oil. Pipe was removed and blinded off. Pipe has been sent in to a lab for future analysis. The pipe that was involved in the accident was a prover line that went 3 foot below ground. Suncor believes that this was a point for water dropout and the pipe has internal corrsion from the water drop out.
Report Received Date 2012-12-06 00:00:00
Iyear 2012
Report Number 20120351
Supplemental Number 18433
Report Type Supplemental Final
Operator Id 31822 PHMSA Enforcement
Name Suncor Energy (Usa) Pipeline Co.
Operator Street Address 1700 Cutler Rd.
Operator City Name Cheyenne
Operator State Abbreviation WY
Operator Postal Code 82001
Local Datetime 2012-11-23 10:30:00
Location Latitude 42.225925 Google Maps OpenStreetMap
Location Longitude -104.686441 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 20
Recovered Bbls 15
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2012-11-23 10:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Leak On Blend Pump Prover Line; Contained In Tank 1 Dike
On Site Datetime 2012-11-23 10:40:00
Nrc Rpt Datetime 2012-11-26 10:00:00
Nrc Rpt Num 1031540 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Guernsey Pump Station
Segment Name Cennenial / 3965
Onshore State Abbreviation Wy
Onshore Postal Code 82214
Onshore City Name Guernsey
Onshore County Name Platte
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4.5
Pipe Wall Thickness 0.237
Pipe Smys 42000
Pipe Specification Api 5l-X42
Pipe Seam Type Seamless
Pipe Manufacturer United States Steel
Pipe Coating Type Extruded Polyehylene
Installation Year 2004
Manufactured Year 2004
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 500
Est Cost Prop Damage 5000
Est Cost Emergency 0
Est Cost Environmental 10000
Est Cost Other 0
Prpty 15500
Accident Psig 180
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pipe was upstream of mainline leak detection system. No abnormal operating conditions were involved.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name L**** H******
Preparer Title Manager- Regulatory Complaince- Row - Training
Preparer Email L*******@s*****.com
Preparer Telephone 3077758101
Preparer Fax 3076376633
Prepared Date 2013-08-09 00:00:00
Authorizer Name L**** H******
Authorizer Telephone 3077758101
Authorizer Title Manager- Regulatory Complaince- Row - Training
Authorizer Email L*******@s*****.com
Narrative Local station operator was making a daily tour of the station and found oil coming up from the ground. He then called the control center to shut down the blend and start pumping out of another tank. He then contacted a contractor with a vacuum truck to pick up oil. Then he contacted a dirt contractor to come and dig up location of the spill to find the source of the oil. Pipe was removed and blinded off. Pipe has been sent in to a lab for future analysis. The pipe that was involved in the accident was a prover line that went 3 foot below ground. Suncor believes that this was a point for water dropout and the pipe has internal corrsion from the water drop out.

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