Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2012-11-12 — TX
Operator
Sunoco Pipeline L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$10,000
Incident datetime
2012-11-12 15:00
Report number
Location
TX
Narrative
Internal corrosion on 10" manifold piping. Affected piping removed and replaced with new pipe. Re-submitted on 3/20/2013 to include part e5f per PHMSA request.
Detailed record list
Report Received Date
2012-12-05 00:00:00
Iyear
2012
Report Number
20120350
Supplemental Number
17636
Report Type
Supplemental Final
Operator Id
18718
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-11-12 15:00:00
Location Latitude
30.28649
Location Longitude
-94.50634
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-11-12 15:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-11-12 15:00:00
Restart Datetime
2012-11-16 14:15:00
On Site Datetime
2012-11-12 15:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Saratoga Station
Segment Name
Manifold Piping
Onshore State Abbreviation
Tx
Onshore Postal Code
77585
Onshore City Name
Saratoga
Onshore County Name
Hardin
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Release Type
Leak
Leak Type
Pinhole
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
41
Est Cost Prop Damage
10000
Est Cost Emergency
1000
Est Cost Environmental
1000
Est Cost Other
0
Prpty
12041
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Preparer Name
T*** N*******
Preparer Title
Dot Compliance Specialist
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
281-637-6425
Prepared Date
2013-03-20 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Specialist
Authorizer Email
T*********@s**************.com
Narrative
Internal corrosion on 10" manifold piping. Affected piping removed and replaced with new pipe. Re-submitted on 3/20/2013 to include part e5f per PHMSA request.
| Report Received Date | 2012-12-05 00:00:00 |
|---|---|
| Iyear | 2012 |
| Report Number | 20120350 |
| Supplemental Number | 17636 |
| Report Type | Supplemental Final |
| Operator Id | 18718 PHMSA Enforcement |
| Name | Sunoco Pipeline L.p. |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2012-11-12 15:00:00 |
| Location Latitude | 30.28649 Google Maps OpenStreetMap |
| Location Longitude | -94.50634 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.5 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2012-11-12 15:00:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2012-11-12 15:00:00 |
| Restart Datetime | 2012-11-16 14:15:00 |
| On Site Datetime | 2012-11-12 15:00:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Saratoga Station |
| Segment Name | Manifold Piping |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77585 |
| Onshore City Name | Saratoga |
| Onshore County Name | Hardin |
| Designated Location | Survey Station No. |
| Designated Name | 0+00 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Intrastate |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Release Type | Leak |
| Leak Type | Pinhole |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 41 |
| Est Cost Prop Damage | 10000 |
| Est Cost Emergency | 1000 |
| Est Cost Environmental | 1000 |
| Est Cost Other | 0 |
| Prpty | 12041 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | Internal Corrosion |
| Internal External | Internal Corrosion |
| Preparer Name | T*** N******* |
| Preparer Title | Dot Compliance Specialist |
| Preparer Email | T*********@s**************.com |
| Preparer Telephone | 281-637-6576 |
| Preparer Fax | 281-637-6425 |
| Prepared Date | 2013-03-20 00:00:00 |
| Authorizer Name | T*** N******* |
| Authorizer Telephone | 281-637-6576 |
| Authorizer Title | Dot Compliance Specialist |
| Authorizer Email | T*********@s**************.com |
| Narrative | Internal corrosion on 10" manifold piping. Affected piping removed and replaced with new pipe. Re-submitted on 3/20/2013 to include part e5f per PHMSA request. |
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