HL incident on 2012-11-02 — TX

Operator
Calnev Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2012-11-02 13:33
Report number
Location
TX
Narrative
On 11/2 the barstow maintenance technician discovered a leak (dripping) on the 8' ml pump, unit #2 discharge valve from around the stem and caused a stain on the soil approximately 36' x 40'. The maintenance technician placed a pan under the valve to contain the drips. The pump was shut down by the orange controller and isolated which stopped the drip. Notifications were made. The unit was locked out of service pending repairs. All contaminated soil was placed into a drum for disposal. A remediation contractor conducted a site evaluation on 11/7 and calculated the spill volume to be 28 gallons (0.67 bbls). The cause of the drip was o-ring seal failure. Note: part a, #14 pump unit #2 was shut down and isolated to stop the leak. The mainline was not shut down for this incident.
Detailed record list
Report Received Date
2012-11-30 00:00:00
Iyear
2012
Report Number
20120342
Supplemental Number
18322
Report Type
Supplemental Final
Operator Id
Name
Calnev Pipeline Co
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-11-02 13:33:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.67
Intentional Release Bbls
0
Recovered Bbls
0.67
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-11-02 13:33:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Unit#2 Only Shut Down & Isolated, Stopping The Drip. Mainline Not Shut Down.
On Site Datetime
2012-11-02 13:33:00
Nrc Rpt Datetime
2012-11-02 13:52:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Baker Pump Station
Onshore State Abbreviation
Ca
Onshore Postal Code
92309
Onshore City Name
Baker
Onshore County Name
San Bernardino
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
84
Est Cost Prop Damage
1000
Est Cost Emergency
500
Est Cost Environmental
6000
Est Cost Other
0
Prpty
7584
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Preparer Name
S**** M*******
Preparer Title
Mgr - Ccs
Preparer Email
S*************@k***********.com
Preparer Telephone
909-873-5146
Preparer Fax
303-984-3620
Prepared Date
2013-07-29 00:00:00
Authorizer Name
E***** A* F***
Authorizer Telephone
713-369-9454
Authorizer Title
Director - Ccs
Authorizer Email
B********@k***********.com
Narrative
On 11/2 the barstow maintenance technician discovered a leak (dripping) on the 8' ml pump, unit #2 discharge valve from around the stem and caused a stain on the soil approximately 36' x 40'. The maintenance technician placed a pan under the valve to contain the drips. The pump was shut down by the orange controller and isolated which stopped the drip. Notifications were made. The unit was locked out of service pending repairs. All contaminated soil was placed into a drum for disposal. A remediation contractor conducted a site evaluation on 11/7 and calculated the spill volume to be 28 gallons (0.67 bbls). The cause of the drip was o-ring seal failure. Note: part a, #14 pump unit #2 was shut down and isolated to stop the leak. The mainline was not shut down for this incident.
Report Received Date 2012-11-30 00:00:00
Iyear 2012
Report Number 20120342
Supplemental Number 18322
Report Type Supplemental Final
Operator Id 26125 PHMSA Enforcement
Name Calnev Pipeline Co
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2012-11-02 13:33:00
Location Latitude 35.276957 Google Maps OpenStreetMap
Location Longitude -116.021774 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.67
Intentional Release Bbls 0
Recovered Bbls 0.67
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2012-11-02 13:33:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Unit#2 Only Shut Down & Isolated, Stopping The Drip. Mainline Not Shut Down.
On Site Datetime 2012-11-02 13:33:00
Nrc Rpt Datetime 2012-11-02 13:52:00
Nrc Rpt Num 1029383 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Baker Pump Station
Onshore State Abbreviation Ca
Onshore Postal Code 92309
Onshore City Name Baker
Onshore County Name San Bernardino
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 84
Est Cost Prop Damage 1000
Est Cost Emergency 500
Est Cost Environmental 6000
Est Cost Other 0
Prpty 7584
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Preparer Name S**** M*******
Preparer Title Mgr - Ccs
Preparer Email S*************@k***********.com
Preparer Telephone 909-873-5146
Preparer Fax 303-984-3620
Prepared Date 2013-07-29 00:00:00
Authorizer Name E***** A* F***
Authorizer Telephone 713-369-9454
Authorizer Title Director - Ccs
Authorizer Email B********@k***********.com
Narrative On 11/2 the barstow maintenance technician discovered a leak (dripping) on the 8' ml pump, unit #2 discharge valve from around the stem and caused a stain on the soil approximately 36' x 40'. The maintenance technician placed a pan under the valve to contain the drips. The pump was shut down by the orange controller and isolated which stopped the drip. Notifications were made. The unit was locked out of service pending repairs. All contaminated soil was placed into a drum for disposal. A remediation contractor conducted a site evaluation on 11/7 and calculated the spill volume to be 28 gallons (0.67 bbls). The cause of the drip was o-ring seal failure. Note: part a, #14 pump unit #2 was shut down and isolated to stop the leak. The mainline was not shut down for this incident.

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