Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2012-11-02 — OK
Operator
Bkep Crude, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$800
Incident datetime
2012-11-02 08:00
Report number
Location
OK
Narrative
No narrative available.
Detailed record list
Report Received Date
2012-11-30 00:00:00
Iyear
2012
Report Number
20120341
Supplemental Number
19598
Report Type
Supplemental Final
Operator Id
32481
Name
Bkep Crude, Llc
Operator Street Address
6060 American Plaza Suite 600
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74135
Local Datetime
2012-11-02 08:00:00
Location Latitude
35.94805
Location Longitude
-96.74979
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.6
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-11-02 08:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Occurred On Metering Skid, Did Not Require Shutdown
On Site Datetime
2012-11-02 08:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Eagle
Segment Name
Eagle
Onshore State Abbreviation
Ok
Onshore Postal Code
74032
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Survey Station No.
Designated Name
South Tankfar
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Meter/prover
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
48
Est Cost Prop Damage
800
Est Cost Emergency
2800
Est Cost Environmental
0
Est Cost Other
0
Prpty
3648
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
R***** S*****
Preparer Title
Mgr Env And Dot Pipeline
Preparer Email
R******@b***.com
Preparer Telephone
5129040788
Preparer Fax
9182374001
Prepared Date
2014-07-25 00:00:00
Authorizer Name
R***** S*****
Authorizer Telephone
5129040788
Authorizer Title
Mgr Env And Dot Pipeline
Authorizer Email
R******@b***.com
| Report Received Date | 2012-11-30 00:00:00 |
|---|---|
| Iyear | 2012 |
| Report Number | 20120341 |
| Supplemental Number | 19598 |
| Report Type | Supplemental Final |
| Operator Id | 32481 PHMSA Enforcement |
| Name | Bkep Crude, Llc |
| Operator Street Address | 6060 American Plaza Suite 600 |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74135 |
| Local Datetime | 2012-11-02 08:00:00 |
| Location Latitude | 35.94805 Google Maps OpenStreetMap |
| Location Longitude | -96.74979 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.6 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2012-11-02 08:00:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Leak Occurred On Metering Skid, Did Not Require Shutdown |
| On Site Datetime | 2012-11-02 08:30:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Eagle |
| Segment Name | Eagle |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 74032 |
| Onshore City Name | Cushing |
| Onshore County Name | Payne |
| Designated Location | Survey Station No. |
| Designated Name | South Tankfar |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Intrastate |
| Item Involved | Meter/prover |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 48 |
| Est Cost Prop Damage | 800 |
| Est Cost Emergency | 2800 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 3648 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Preparer Name | R***** S***** |
| Preparer Title | Mgr Env And Dot Pipeline |
| Preparer Email | R******@b***.com |
| Preparer Telephone | 5129040788 |
| Preparer Fax | 9182374001 |
| Prepared Date | 2014-07-25 00:00:00 |
| Authorizer Name | R***** S***** |
| Authorizer Telephone | 5129040788 |
| Authorizer Title | Mgr Env And Dot Pipeline |
| Authorizer Email | R******@b***.com |
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