HL incident on 2012-10-30 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,500
Incident datetime
2012-10-30 11:57
Report number
Location
TX
Narrative
A very small leak was found, approximately 10 gallons of propane, during a excavation on the blue line to evaluate an anomaly. The leak was near madison, ks in a very remote site. 2015-2-17 - various sections and questions updated to reflect new report requirements.
Detailed record list
Report Received Date
2012-11-28 00:00:00
Iyear
2012
Report Number
20120333
Supplemental Number
20214
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2012-10-30 11:57:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.24
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2012-10-30 11:57:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-10-30 11:57:00
Restart Datetime
2012-10-30 17:04:00
On Site Datetime
2012-10-30 11:57:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Blue Line
Segment Name
Cassoday To Sharpe
Onshore State Abbreviation
Ks
Onshore Postal Code
66860
Onshore City Name
Madison
Onshore County Name
Greenwood
Designated Location
Milepost/valve Station
Designated Name
Mp 339
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
30
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12.75
Pipe Wall Thickness
0.25
Pipe Smys
45000
Pipe Specification
Api 5lx
Pipe Seam Type
Flash Welded
Pipe Manufacturer
Ao Smith
Pipe Coating Type
Coal Tar
Installation Year
1952
Manufactured Year
1952
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
3500
Est Cost Emergency
200
Est Cost Environmental
100
Est Cost Other
0
Prpty
3820
Accident Psig
250
Mop Psig
1218
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
69704
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak size and rate undetectable by scada. Controller actions did not contribute to this release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Stray Current Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1952
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2012
Close Interval Survey Year
2012
Prior Damage
No
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Axial Recent Year
2008
Geometry Recent Year
2008
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1980
Hydrtst Most Rcnt Pressure
1405
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
J*** B*********
Preparer Title
Dot Coordinator
Preparer Email
J**************@p**.com
Preparer Telephone
918-977-4206
Preparer Fax
918-661-3381
Prepared Date
2015-03-06 00:00:00
Authorizer Name
T*** T*****
Authorizer Telephone
832-765-1636
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
T************@p**.com
Narrative
A very small leak was found, approximately 10 gallons of propane, during a excavation on the blue line to evaluate an anomaly. The leak was near madison, ks in a very remote site. 2015-2-17 - various sections and questions updated to reflect new report requirements.
Report Received Date 2012-11-28 00:00:00
Iyear 2012
Report Number 20120333
Supplemental Number 20214
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2012-10-30 11:57:00
Location Latitude 38.12745 Google Maps OpenStreetMap
Location Longitude -96.191081 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.24
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2012-10-30 11:57:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-10-30 11:57:00
Restart Datetime 2012-10-30 17:04:00
On Site Datetime 2012-10-30 11:57:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Blue Line
Segment Name Cassoday To Sharpe
Onshore State Abbreviation Ks
Onshore Postal Code 66860
Onshore City Name Madison
Onshore County Name Greenwood
Designated Location Milepost/valve Station
Designated Name Mp 339
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 30
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12.75
Pipe Wall Thickness 0.25
Pipe Smys 45000
Pipe Specification Api 5lx
Pipe Seam Type Flash Welded
Pipe Manufacturer Ao Smith
Pipe Coating Type Coal Tar
Installation Year 1952
Manufactured Year 1952
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 3500
Est Cost Emergency 200
Est Cost Environmental 100
Est Cost Other 0
Prpty 3820
Accident Psig 250
Mop Psig 1218
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 69704
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak size and rate undetectable by scada. Controller actions did not contribute to this release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Stray Current Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1952
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2012
Close Interval Survey Year 2012
Prior Damage No
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Axial Recent Year 2008
Geometry Recent Year 2008
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1980
Hydrtst Most Rcnt Pressure 1405
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name J*** B*********
Preparer Title Dot Coordinator
Preparer Email J**************@p**.com
Preparer Telephone 918-977-4206
Preparer Fax 918-661-3381
Prepared Date 2015-03-06 00:00:00
Authorizer Name T*** T*****
Authorizer Telephone 832-765-1636
Authorizer Title Regulatory Compliance Manager
Authorizer Email T************@p**.com
Narrative A very small leak was found, approximately 10 gallons of propane, during a excavation on the blue line to evaluate an anomaly. The leak was near madison, ks in a very remote site. 2015-2-17 - various sections and questions updated to reflect new report requirements.

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