HL incident on 2012-10-14 — TX

Operator
Mustang Pipe Line Partners
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2012-10-14 11:20
Report number
Location
TX
Narrative
The mustang pipeline system experienced a 1.5 barrel crude release at gibson city, ford county, illinois. Incident was inside the pump room building and 40 gallon reached soil outside the building and 23 gallon was removed inside the building. Emergency notification was made to the nrc, illinois emergency management, local lepc/sheriff and US epa region v. Empco employee began clean-up release immediately on arrival at site after notification was completed. Phmsa- follows up call with karen butler at @ 2:30 pm. On 10-14-12 all impacted soil was clean up and transported to an exxonmobil approved waste site. The seal failed due to excessive wear on pump internals. This led to an excessive amount of movement of the shaft during pump operation. 1-08-2013- supplemental report submitted final clean-up completed and environmental clean-up was less than projected in on original 7001 submitted report. 7-31-13 supplemental report PHMSA requested supplemental be created to added part e 5 f data ie, ( function of pipeline system) be added to form.
Detailed record list
Report Received Date
2012-11-12 00:00:00
Iyear
2012
Report Number
20120321
Supplemental Number
18374
Report Type
Supplemental Final
Operator Id
Name
Mustang Pipe Line Partners
Operator Street Address
22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2012-10-14 11:20:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.5
Intentional Release Bbls
0
Recovered Bbls
1.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2012-10-14 11:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pump Station Was Isolated From The Pipeline & Pipeline Continued Full Operation
On Site Datetime
2012-10-14 11:30:00
Nrc Rpt Datetime
2012-10-14 11:30:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Gibson City Pump Station- Mustang Crude System
Segment Name
Mokena To Patoka 18" Crude System
Onshore State Abbreviation
Il
Onshore Postal Code
60936
Onshore City Name
Gibson City
Onshore County Name
Ford
Designated Location
Milepost/valve Station
Designated Name
Gibson City
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
1950
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
135
Est Cost Prop Damage
0
Est Cost Emergency
15000
Est Cost Environmental
60284
Est Cost Other
0
Prpty
75419
Accident Psig
500
Mop Psig
760
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Field mechanical failure was cause of the leak and activated a cse ( critical safety equipment) the control room promptly reported the activation of the cse to field operations
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
The Seal Failed Due To Excessive Wear On Pump Internals .
Preparer Name
L**** E H********
Preparer Title
Pipeline Safety Advisor
Preparer Email
L****************@e*********.com
Preparer Telephone
903-654-5345
Preparer Fax
903-654-5374
Prepared Date
2013-07-31 00:00:00
Authorizer Name
M**** D* W******
Authorizer Telephone
713-656-0227
Authorizer Title
S H E Manager
Authorizer Email
M*************@e*********.com
Narrative
T****************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ 2:30 pm. On 10-14-12 all impacted soil was clean up and transported to an exxonmobil approved waste site. The seal failed due to excessive wear on pump internals. This led to an excessive amount of movement of the shaft during pump operation. 1-08-2013- supplemental report submitted final clean-up completed and environmental clean-up was less than projected in on original 7001 submitted report. *******************************************************************************************************************************************************.
Report Received Date 2012-11-12 00:00:00
Iyear 2012
Report Number 20120321
Supplemental Number 18374
Report Type Supplemental Final
Operator Id 31166 PHMSA Enforcement
Name Mustang Pipe Line Partners
Operator Street Address 22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Local Datetime 2012-10-14 11:20:00
Location Latitude 40.51608 Google Maps OpenStreetMap
Location Longitude -88.31929 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.5
Intentional Release Bbls 0
Recovered Bbls 1.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2012-10-14 11:20:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pump Station Was Isolated From The Pipeline & Pipeline Continued Full Operation
On Site Datetime 2012-10-14 11:30:00
Nrc Rpt Datetime 2012-10-14 11:30:00
Nrc Rpt Num 1027279 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Gibson City Pump Station- Mustang Crude System
Segment Name Mokena To Patoka 18" Crude System
Onshore State Abbreviation Il
Onshore Postal Code 60936
Onshore City Name Gibson City
Onshore County Name Ford
Designated Location Milepost/valve Station
Designated Name Gibson City
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 1950
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 135
Est Cost Prop Damage 0
Est Cost Emergency 15000
Est Cost Environmental 60284
Est Cost Other 0
Prpty 75419
Accident Psig 500
Mop Psig 760
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Field mechanical failure was cause of the leak and activated a cse ( critical safety equipment) the control room promptly reported the activation of the cse to field operations
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details The Seal Failed Due To Excessive Wear On Pump Internals .
Preparer Name L**** E H********
Preparer Title Pipeline Safety Advisor
Preparer Email L****************@e*********.com
Preparer Telephone 903-654-5345
Preparer Fax 903-654-5374
Prepared Date 2013-07-31 00:00:00
Authorizer Name M**** D* W******
Authorizer Telephone 713-656-0227
Authorizer Title S H E Manager
Authorizer Email M*************@e*********.com
Narrative T****************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ 2:30 pm. On 10-14-12 all impacted soil was clean up and transported to an exxonmobil approved waste site. The seal failed due to excessive wear on pump internals. This led to an excessive amount of movement of the shaft during pump operation. 1-08-2013- supplemental report submitted final clean-up completed and environmental clean-up was less than projected in on original 7001 submitted report. *******************************************************************************************************************************************************.

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