Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2012-10-14 — TX
Operator
Mustang Pipe Line Partners
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2012-10-14 11:20
Report number
Location
TX
Narrative
The mustang pipeline system experienced a 1.5 barrel crude release at gibson city, ford county, illinois. Incident was inside the pump room building and 40 gallon reached soil outside the building and 23 gallon was removed inside the building. Emergency notification was made to the nrc, illinois emergency management, local lepc/sheriff and US epa region v. Empco employee began clean-up release immediately on arrival at site after notification was completed. Phmsa- follows up call with karen butler at @ 2:30 pm. On 10-14-12 all impacted soil was clean up and transported to an exxonmobil approved waste site. The seal failed due to excessive wear on pump internals. This led to an excessive amount of movement of the shaft during pump operation. 1-08-2013- supplemental report submitted final clean-up completed and environmental clean-up was less than projected in on original 7001 submitted report. 7-31-13 supplemental report PHMSA requested supplemental be created to added part e 5 f data ie, ( function of pipeline system) be added to form.
Detailed record list
Report Received Date
2012-11-12 00:00:00
Iyear
2012
Report Number
20120321
Supplemental Number
18374
Report Type
Supplemental Final
Operator Id
31166
Name
Mustang Pipe Line Partners
Operator Street Address
22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2012-10-14 11:20:00
Location Latitude
40.51608
Location Longitude
-88.31929
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.5
Intentional Release Bbls
0
Recovered Bbls
1.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2012-10-14 11:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pump Station Was Isolated From The Pipeline & Pipeline Continued Full Operation
On Site Datetime
2012-10-14 11:30:00
Nrc Rpt Datetime
2012-10-14 11:30:00
Nrc Rpt Num
1027279
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Gibson City Pump Station- Mustang Crude System
Segment Name
Mokena To Patoka 18" Crude System
Onshore State Abbreviation
Il
Onshore Postal Code
60936
Onshore City Name
Gibson City
Onshore County Name
Ford
Designated Location
Milepost/valve Station
Designated Name
Gibson City
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
1950
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
135
Est Cost Prop Damage
0
Est Cost Emergency
15000
Est Cost Environmental
60284
Est Cost Other
0
Prpty
75419
Accident Psig
500
Mop Psig
760
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Field mechanical failure was cause of the leak and activated a cse ( critical safety equipment) the control room promptly reported the activation of the cse to field operations
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
The Seal Failed Due To Excessive Wear On Pump Internals .
Preparer Name
L**** E H********
Preparer Title
Pipeline Safety Advisor
Preparer Email
L****************@e*********.com
Preparer Telephone
903-654-5345
Preparer Fax
903-654-5374
Prepared Date
2013-07-31 00:00:00
Authorizer Name
M**** D* W******
Authorizer Telephone
713-656-0227
Authorizer Title
S H E Manager
Authorizer Email
M*************@e*********.com
Narrative
T****************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ 2:30 pm. On 10-14-12 all impacted soil was clean up and transported to an exxonmobil approved waste site. The seal failed due to excessive wear on pump internals. This led to an excessive amount of movement of the shaft during pump operation. 1-08-2013- supplemental report submitted final clean-up completed and environmental clean-up was less than projected in on original 7001 submitted report. *******************************************************************************************************************************************************.
| Report Received Date | 2012-11-12 00:00:00 |
|---|---|
| Iyear | 2012 |
| Report Number | 20120321 |
| Supplemental Number | 18374 |
| Report Type | Supplemental Final |
| Operator Id | 31166 PHMSA Enforcement |
| Name | Mustang Pipe Line Partners |
| Operator Street Address | 22777 Springwoods Village Parkway E2.2b-Emp |
| Operator City Name | Spring |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77389 |
| Local Datetime | 2012-10-14 11:20:00 |
| Location Latitude | 40.51608 Google Maps OpenStreetMap |
| Location Longitude | -88.31929 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 1.5 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 1.5 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations) |
| Incident Identified Datetime | 2012-10-14 11:20:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Pump Station Was Isolated From The Pipeline & Pipeline Continued Full Operation |
| On Site Datetime | 2012-10-14 11:30:00 |
| Nrc Rpt Datetime | 2012-10-14 11:30:00 |
| Nrc Rpt Num | 1027279 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Gibson City Pump Station- Mustang Crude System |
| Segment Name | Mokena To Patoka 18" Crude System |
| Onshore State Abbreviation | Il |
| Onshore Postal Code | 60936 |
| Onshore City Name | Gibson City |
| Onshore County Name | Ford |
| Designated Location | Milepost/valve Station |
| Designated Name | Gibson City |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Inside A Building |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Pump |
| Installation Year | 1950 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 135 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 15000 |
| Est Cost Environmental | 60284 |
| Est Cost Other | 0 |
| Prpty | 75419 |
| Accident Psig | 500 |
| Mop Psig | 760 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | Yes |
| Scada Conf Ind | Yes |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | Yes |
| Cpm Conf Ind | Yes |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Field mechanical failure was cause of the leak and activated a cse ( critical safety equipment) the control room promptly reported the activation of the cse to field operations |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Pump Or Pump-Related Equipment |
| Eq Failure Type | Pump Or Pump-Related Equipment |
| Other Pump Ind | Seal/packing Failure |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | The Seal Failed Due To Excessive Wear On Pump Internals . |
| Preparer Name | L**** E H******** |
| Preparer Title | Pipeline Safety Advisor |
| Preparer Email | L****************@e*********.com |
| Preparer Telephone | 903-654-5345 |
| Preparer Fax | 903-654-5374 |
| Prepared Date | 2013-07-31 00:00:00 |
| Authorizer Name | M**** D* W****** |
| Authorizer Telephone | 713-656-0227 |
| Authorizer Title | S H E Manager |
| Authorizer Email | M*************@e*********.com |
| Narrative | T****************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ 2:30 pm. On 10-14-12 all impacted soil was clean up and transported to an exxonmobil approved waste site. The seal failed due to excessive wear on pump internals. This led to an excessive amount of movement of the shaft during pump operation. 1-08-2013- supplemental report submitted final clean-up completed and environmental clean-up was less than projected in on original 7001 submitted report. *******************************************************************************************************************************************************. |
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