Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2012-10-13 — OK
Operator
Magellan Terminals Holdings, Lp
Cause
Natural Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2012-10-13 17:30
Report number
Location
OK
Narrative
During a severe weaher event, a plywood form was picked up by the wind and tossed into a 3/4" fitting on the piping. The strike caused the fitting to break allowing crude to be released. The line was immediately shut down. The spill was cleaned up and a new 3/4" plug was installed.
Detailed record list
Report Received Date
2012-10-31 00:00:00
Iyear
2012
Report Number
20120313
Supplemental Number
17379
Report Type
Supplemental Final
Operator Id
31580
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2012-10-13 17:30:00
Location Latitude
35.94109
Location Longitude
-96.74697
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Intentional Release Bbls
0
Recovered Bbls
0.98
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-10-13 17:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-10-13 17:30:00
Restart Datetime
2012-10-13 22:15:00
On Site Datetime
2012-10-13 17:45:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing Central Crude
Segment Name
Pipe Segment
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Lincoln
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Release Type
Other
Release Type Details
Debris Struck A Fitting During A Storm Breaking The Fitting Loose
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
17000
Est Cost Environmental
0
Est Cost Other
0
Prpty
17000
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
High Winds
Natural Force Type
High Winds
Nf Extreme Weather Ind
Yes
Nf Other Ind
Yes
Nf Extreme Weather Details
60 Mph Winds During A Storm
Preparer Name
D******* C*********
Preparer Title
Sr Compliance Coordinator
Preparer Email
D******************@m*********.com
Preparer Telephone
918-574-7386
Prepared Date
2013-03-06 00:00:00
Authorizer Name
D******* C*********
Authorizer Telephone
918-574-7386
Authorizer Email
No Email Address
Narrative
During a severe weaher event, a plywood form was picked up by the wind and tossed into a 3/4" fitting on the piping. The strike caused the fitting to break allowing crude to be released. The line was immediately shut down. The spill was cleaned up and a new 3/4" plug was installed.
| Report Received Date | 2012-10-31 00:00:00 |
|---|---|
| Iyear | 2012 |
| Report Number | 20120313 |
| Supplemental Number | 17379 |
| Report Type | Supplemental Final |
| Operator Id | 31580 PHMSA Enforcement |
| Name | Magellan Terminals Holdings, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2012-10-13 17:30:00 |
| Location Latitude | 35.94109 Google Maps OpenStreetMap |
| Location Longitude | -96.74697 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 1 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0.98 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2012-10-13 17:30:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2012-10-13 17:30:00 |
| Restart Datetime | 2012-10-13 22:15:00 |
| On Site Datetime | 2012-10-13 17:45:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Cushing Central Crude |
| Segment Name | Pipe Segment |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 74023 |
| Onshore City Name | Cushing |
| Onshore County Name | Lincoln |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Auxiliary Piping (E.g. Drain Lines) |
| Release Type | Other |
| Release Type Details | Debris Struck A Fitting During A Storm Breaking The Fitting Loose |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 0 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 17000 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 17000 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Natural Force Damage |
| Cause Details | High Winds |
| Natural Force Type | High Winds |
| Nf Extreme Weather Ind | Yes |
| Nf Other Ind | Yes |
| Nf Extreme Weather Details | 60 Mph Winds During A Storm |
| Preparer Name | D******* C********* |
| Preparer Title | Sr Compliance Coordinator |
| Preparer Email | D******************@m*********.com |
| Preparer Telephone | 918-574-7386 |
| Prepared Date | 2013-03-06 00:00:00 |
| Authorizer Name | D******* C********* |
| Authorizer Telephone | 918-574-7386 |
| Authorizer Email | No Email Address |
| Narrative | During a severe weaher event, a plywood form was picked up by the wind and tossed into a 3/4" fitting on the piping. The strike caused the fitting to break allowing crude to be released. The line was immediately shut down. The spill was cleaned up and a new 3/4" plug was installed. |
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