HL incident on 2012-09-27 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$300
Incident datetime
2012-09-27 13:00
Report number
Location
TX
Narrative
During commissioning operations at 1 pm on sept 27 at cowden station, a 1.5" gate valve on a strainer failed to hold while the line was being filled. Flow through this valve emptied into the station sump, and after filling the sump overflowed. About 1.5 barrels of crude were spilled.
Detailed record list
Report Received Date
2012-10-24 00:00:00
Iyear
2012
Report Number
20120307
Supplemental Number
17939
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-09-27 13:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.5
Intentional Release Bbls
0
Recovered Bbls
1.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Gate Valve Replaced Within Hours
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Cowden Station
Onshore State Abbreviation
Tx
Onshore Postal Code
79707
Onshore City Name
Midland
Onshore County Name
Martin
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Sump
Release Type
Overfill Or Overflow
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
150
Est Cost Prop Damage
300
Est Cost Emergency
0
Est Cost Environmental
600
Est Cost Other
0
Prpty
1050
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Preparer Name
C********** H****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
C******@e****.com
Preparer Telephone
713-381-6304
Prepared Date
2013-04-25 00:00:00
Authorizer Name
C********** H****
Authorizer Telephone
713-381-6304
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
C******@e****.com
Narrative
During commissioning operations at 1 pm on sept 27 at cowden station, a 1.5" gate valve on a strainer failed to hold while the line was being filled. Flow through this valve emptied into the station sump, and after filling the sump overflowed. About 1.5 barrels of crude were spilled.
Report Received Date 2012-10-24 00:00:00
Iyear 2012
Report Number 20120307
Supplemental Number 17939
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2012-09-27 13:00:00
Location Latitude 32.089083 Google Maps OpenStreetMap
Location Longitude -102.138981 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.5
Intentional Release Bbls 0
Recovered Bbls 1.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Gate Valve Replaced Within Hours
Ignite Ind No
Explode Ind No
Pipe Fac Name Cowden Station
Onshore State Abbreviation Tx
Onshore Postal Code 79707
Onshore City Name Midland
Onshore County Name Martin
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Intrastate
Item Involved Sump
Release Type Overfill Or Overflow
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 150
Est Cost Prop Damage 300
Est Cost Emergency 0
Est Cost Environmental 600
Est Cost Other 0
Prpty 1050
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Preparer Name C********** H****
Preparer Title Pipeline Compliance Engineer
Preparer Email C******@e****.com
Preparer Telephone 713-381-6304
Prepared Date 2013-04-25 00:00:00
Authorizer Name C********** H****
Authorizer Telephone 713-381-6304
Authorizer Title Pipeline Compliance Engineer
Authorizer Email C******@e****.com
Narrative During commissioning operations at 1 pm on sept 27 at cowden station, a 1.5" gate valve on a strainer failed to hold while the line was being filled. Flow through this valve emptied into the station sump, and after filling the sump overflowed. About 1.5 barrels of crude were spilled.

All rights reserved. Copyright © by ClearPHMSA