HL incident on 2012-09-21 — TX

Operator
Plains Marketing, L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,000
Incident datetime
2012-09-21 08:30
Report number
Location
TX
Narrative
Approximately 2.9 barrels of crude oil was released due to crevice corrosion between an angle iron stairway support attachment weld and the tank shell. Water and condensation had become trapped between the angle iron stairway support and tank shell, causing the coating to deteriorate and crevice corrosion to form at the attachment weld and shell. Porosity trapped in the weld and burn through may also have contributed to the pinhole leak. The pinhole leak was located on the .250" thick carbon steel plate of the top shell course. The affected area was not in a vertical or circumferential weld seam.
Detailed record list
Report Received Date
2012-10-18 00:00:00
Iyear
2012
Report Number
20120301
Supplemental Number
17701
Report Type
Supplemental Final
Operator Id
Name
Plains Marketing, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-09-21 08:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2.9
Intentional Release Bbls
0
Recovered Bbls
2.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-09-21 08:30:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Release - Shutdown Not Necessary
On Site Datetime
2012-09-21 09:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
El Segundo
Onshore State Abbreviation
Ca
Onshore Postal Code
90245
Onshore City Name
El Segundo
Onshore County Name
Los Angeles
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Type
Atmospheric
Release Type
Leak
Leak Type
Pinhole
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
25000
Est Cost Emergency
20000
Est Cost Environmental
0
Est Cost Other
0
Prpty
45000
Pipeline Function
< 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Preparer Name
S***** N*****
Preparer Title
Compliance Specialist
Preparer Email
S******@p****.com
Preparer Telephone
713-993-5673
Preparer Fax
713-646-4310
Prepared Date
2013-03-26 00:00:00
Authorizer Name
J***** R J****
Authorizer Telephone
713-993-5162
Authorizer Title
Sr Director Env And Regulatory Compliance
Authorizer Email
J******@p****.com
Narrative
Approximately 2.9 barrels of crude oil was released due to crevice corrosion between an angle iron stairway support attachment weld and the tank shell. Water and condensation had become trapped between the angle iron stairway support and tank shell, causing the coating to deteriorate and crevice corrosion to form at the attachment weld and shell. Porosity trapped in the weld and burn through may also have contributed to the pinhole leak. The pinhole leak was located on the .250" thick carbon steel plate of the top shell course. The affected area was not in a vertical or circumferential weld seam.
Report Received Date 2012-10-18 00:00:00
Iyear 2012
Report Number 20120301
Supplemental Number 17701
Report Type Supplemental Final
Operator Id 26085 PHMSA Enforcement
Name Plains Marketing, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2012-09-21 08:30:00
Location Latitude 33.90593 Google Maps OpenStreetMap
Location Longitude -118.42132 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2.9
Intentional Release Bbls 0
Recovered Bbls 2.9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2012-09-21 08:30:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Release - Shutdown Not Necessary
On Site Datetime 2012-09-21 09:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name El Segundo
Onshore State Abbreviation Ca
Onshore Postal Code 90245
Onshore City Name El Segundo
Onshore County Name Los Angeles
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Type Atmospheric
Release Type Leak
Leak Type Pinhole
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 25000
Est Cost Emergency 20000
Est Cost Environmental 0
Est Cost Other 0
Prpty 45000
Pipeline Function < 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Preparer Name S***** N*****
Preparer Title Compliance Specialist
Preparer Email S******@p****.com
Preparer Telephone 713-993-5673
Preparer Fax 713-646-4310
Prepared Date 2013-03-26 00:00:00
Authorizer Name J***** R J****
Authorizer Telephone 713-993-5162
Authorizer Title Sr Director Env And Regulatory Compliance
Authorizer Email J******@p****.com
Narrative Approximately 2.9 barrels of crude oil was released due to crevice corrosion between an angle iron stairway support attachment weld and the tank shell. Water and condensation had become trapped between the angle iron stairway support and tank shell, causing the coating to deteriorate and crevice corrosion to form at the attachment weld and shell. Porosity trapped in the weld and burn through may also have contributed to the pinhole leak. The pinhole leak was located on the .250" thick carbon steel plate of the top shell course. The affected area was not in a vertical or circumferential weld seam.

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