HL incident on 2012-09-21 — TX

Operator
West Texas Gulf Pipeline Co
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,000
Incident datetime
2012-09-21 14:05
Report number
Location
TX
Narrative
External corrosion on 2" sump line from pump. Line segment replaced with new piping. Re-submitted on 3/20/2013 to include part e5f per PHMSA request.
Detailed record list
Report Received Date
2012-10-17 00:00:00
Iyear
2012
Report Number
20120298
Supplemental Number
17603
Report Type
Supplemental Final
Operator Id
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-09-21 14:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.48
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-09-21 14:05:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Sump Line Isolated By Valve Realignment
On Site Datetime
2012-09-21 14:20:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Colorado City Station
Segment Name
Station Piping-Sump Line
Onshore State Abbreviation
Tx
Onshore Postal Code
79526
Onshore City Name
Hermleigh
Onshore County Name
Scurry
Designated Location
Milepost/valve Station
Designated Name
Colorado City
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Release Type
Leak
Leak Type
Pinhole
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
43
Est Cost Prop Damage
25000
Est Cost Emergency
0
Est Cost Environmental
1500
Est Cost Other
0
Prpty
26543
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Specialist
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
281-637-6425
Prepared Date
2013-03-20 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Specialist
Authorizer Email
T*********@s**************.com
Narrative
External corrosion on 2" sump line from pump. Line segment replaced with new piping. Re-submitted on 3/20/2013 to include part e5f per PHMSA request.
Report Received Date 2012-10-17 00:00:00
Iyear 2012
Report Number 20120298
Supplemental Number 17603
Report Type Supplemental Final
Operator Id 22442 PHMSA Enforcement
Name West Texas Gulf Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2012-09-21 14:00:00
Location Latitude 32.5327 Google Maps OpenStreetMap
Location Longitude -100.8309 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.48
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2012-09-21 14:05:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Sump Line Isolated By Valve Realignment
On Site Datetime 2012-09-21 14:20:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Colorado City Station
Segment Name Station Piping-Sump Line
Onshore State Abbreviation Tx
Onshore Postal Code 79526
Onshore City Name Hermleigh
Onshore County Name Scurry
Designated Location Milepost/valve Station
Designated Name Colorado City
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Release Type Leak
Leak Type Pinhole
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 43
Est Cost Prop Damage 25000
Est Cost Emergency 0
Est Cost Environmental 1500
Est Cost Other 0
Prpty 26543
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Specialist
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 281-637-6425
Prepared Date 2013-03-20 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Specialist
Authorizer Email T*********@s**************.com
Narrative External corrosion on 2" sump line from pump. Line segment replaced with new piping. Re-submitted on 3/20/2013 to include part e5f per PHMSA request.

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