HL incident on 2012-09-11 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,430,918
Incident datetime
2012-09-11 15:10
Report number
Location
TX
Narrative
During walk around operator found stain on ground in dike wall near water draw on tank 170-5. Water draw was isolated and tank emptied. Stain was remediated and tank is out of service for repairs.
Detailed record list
Report Received Date
2012-10-11 00:00:00
Iyear
2012
Report Number
20120293
Supplemental Number
20826
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-09-11 03:10:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.5
Intentional Release Bbls
0
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2012-09-11 15:10:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-09-11 03:10:00
Restart Datetime
2013-03-01 12:00:00
On Site Datetime
2012-09-11 15:15:00
Nrc Rpt Datetime
2012-10-17 15:35:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Pasadena
Segment Name
Tank 170-5
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Single Bottom System
Tank Type
Atmospheric
Api Std Out Of Service Year
2007
Api Std In Service Year
2007
Installation Year
1963
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
2
Est Cost Prop Damage
1430918
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1430920
Accident Psig
150
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The tank was not running at the time the leak was found.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
Topside Of Tank Bottom Plates
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
No
Preparer Name
D******* S*******
Preparer Title
Director - Regulatory Compliance
Preparer Email
D****************@k***********.com
Preparer Telephone
713.725.0147
Preparer Fax
303.984.3048
Prepared Date
2015-10-19 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
713.725.0147
Authorizer Title
Director- Regulatory Compliance
Authorizer Email
D****************@k***********.com
Narrative
During walk around operator found stain on ground in dike wall near water draw on tank 170-5. Water draw was isolated and tank emptied. Stain was remediated and tank is out of service for repairs.
Report Received Date 2012-10-11 00:00:00
Iyear 2012
Report Number 20120293
Supplemental Number 20826
Report Type Supplemental Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2012-09-11 03:10:00
Location Latitude 29.72536 Google Maps OpenStreetMap
Location Longitude -95.20334 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.5
Intentional Release Bbls 0
Recovered Bbls 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2012-09-11 15:10:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-09-11 03:10:00
Restart Datetime 2013-03-01 12:00:00
On Site Datetime 2012-09-11 15:15:00
Nrc Rpt Datetime 2012-10-17 15:35:00
Nrc Rpt Num 1027826 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Pasadena
Segment Name Tank 170-5
Onshore State Abbreviation Tx
Onshore Postal Code 77547
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Vessel Subtype Single Bottom System
Tank Type Atmospheric
Api Std Out Of Service Year 2007
Api Std In Service Year 2007
Installation Year 1963
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 2
Est Cost Prop Damage 1430918
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1430920
Accident Psig 150
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The tank was not running at the time the leak was found.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details Topside Of Tank Bottom Plates
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons No
Preparer Name D******* S*******
Preparer Title Director - Regulatory Compliance
Preparer Email D****************@k***********.com
Preparer Telephone 713.725.0147
Preparer Fax 303.984.3048
Prepared Date 2015-10-19 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 713.725.0147
Authorizer Title Director- Regulatory Compliance
Authorizer Email D****************@k***********.com
Narrative During walk around operator found stain on ground in dike wall near water draw on tank 170-5. Water draw was isolated and tank emptied. Stain was remediated and tank is out of service for repairs.

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