Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2012-09-13 — KS
Operator
Jayhawk Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$500
Incident datetime
2012-09-13 11:45
Report number
Location
KS
Narrative
During routine check of station station operator found that packing had began leaking and created a spill. Pump was shut down and loto'd vac truck was called out to pick up approx. 9 gallons of oil on surface. Liberal personell were dispatched to site and all impacted soils were removed and will be remediated. Mechanic replaced packing in pump. Affected area was 35 feet long by 5 feet wide.Ground was wet from rain so oil did not soak into ground more than an inch or so
Detailed record list
Report Received Date
2012-10-04 00:00:00
Iyear
2012
Report Number
20120285
Supplemental Number
18138
Report Type
Supplemental Final
Operator Id
9175
Name
Jayhawk Pipeline Llc
Operator Street Address
2000 S. Main
Operator City Name
Mcpherson
Operator State Abbreviation
KS
Operator Postal Code
67460
Local Datetime
2012-09-13 11:45:00
Location Latitude
37.6159
Location Longitude
-99.1263
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.38
Intentional Release Bbls
0
Recovered Bbls
0.21
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-09-13 11:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-09-13 11:46:00
Restart Datetime
2012-09-13 17:30:00
On Site Datetime
2012-09-13 11:45:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Haviland Station
Segment Name
Meade To Schurr 12"
Onshore State Abbreviation
Ks
Onshore Postal Code
67059
Onshore City Name
Haviland
Onshore County Name
Kiowa
Designated Location
Milepost/valve Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pump
Release Type
Other
Release Type Details
Pump Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
25
Est Cost Prop Damage
500
Est Cost Emergency
500
Est Cost Environmental
250
Est Cost Other
200
Est Cost Other Details
Vac Truck
Prpty
1475
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
D**** C***
Preparer Title
Operations Manager
Preparer Email
D****@j********.com
Preparer Telephone
6202419260
Preparer Fax
6202419215
Prepared Date
2013-05-29 00:00:00
Authorizer Name
D**** C***
Authorizer Telephone
6202419260
Authorizer Title
Operations Manager
Authorizer Email
D****@j********.com
Narrative
During routine check of station station operator found that packing had began leaking and created a spill. Pump was shut down and loto'd vac truck was called out to pick up approx. 9 gallons of oil on surface. Liberal personell were dispatched to site and all impacted soils were removed and will be remediated. Mechanic replaced packing in pump. Affected area was 35 feet long by 5 feet wide.Ground was wet from rain so oil did not soak into ground more than an inch or so
| Report Received Date | 2012-10-04 00:00:00 |
|---|---|
| Iyear | 2012 |
| Report Number | 20120285 |
| Supplemental Number | 18138 |
| Report Type | Supplemental Final |
| Operator Id | 9175 PHMSA Enforcement |
| Name | Jayhawk Pipeline Llc |
| Operator Street Address | 2000 S. Main |
| Operator City Name | Mcpherson |
| Operator State Abbreviation | KS |
| Operator Postal Code | 67460 |
| Local Datetime | 2012-09-13 11:45:00 |
| Location Latitude | 37.6159 Google Maps OpenStreetMap |
| Location Longitude | -99.1263 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.38 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0.21 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2012-09-13 11:45:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2012-09-13 11:46:00 |
| Restart Datetime | 2012-09-13 17:30:00 |
| On Site Datetime | 2012-09-13 11:45:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Haviland Station |
| Segment Name | Meade To Schurr 12" |
| Onshore State Abbreviation | Ks |
| Onshore Postal Code | 67059 |
| Onshore City Name | Haviland |
| Onshore County Name | Kiowa |
| Designated Location | Milepost/valve Station |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Pump |
| Release Type | Other |
| Release Type Details | Pump Packing |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 25 |
| Est Cost Prop Damage | 500 |
| Est Cost Emergency | 500 |
| Est Cost Environmental | 250 |
| Est Cost Other | 200 |
| Est Cost Other Details | Vac Truck |
| Prpty | 1475 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Pump Or Pump-Related Equipment |
| Eq Failure Type | Pump Or Pump-Related Equipment |
| Preparer Name | D**** C*** |
| Preparer Title | Operations Manager |
| Preparer Email | D****@j********.com |
| Preparer Telephone | 6202419260 |
| Preparer Fax | 6202419215 |
| Prepared Date | 2013-05-29 00:00:00 |
| Authorizer Name | D**** C*** |
| Authorizer Telephone | 6202419260 |
| Authorizer Title | Operations Manager |
| Authorizer Email | D****@j********.com |
| Narrative | During routine check of station station operator found that packing had began leaking and created a spill. Pump was shut down and loto'd vac truck was called out to pick up approx. 9 gallons of oil on surface. Liberal personell were dispatched to site and all impacted soils were removed and will be remediated. Mechanic replaced packing in pump. Affected area was 35 feet long by 5 feet wide.Ground was wet from rain so oil did not soak into ground more than an inch or so |
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