HL incident on 2012-09-09 — OK

Operator
Magellan Ammonia Pipeline, L.p.
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2012-09-09 07:35
Report number
Location
OK
Narrative
Aerial patrol pilot spotted a small area of distressed vegetation in a cultivated field and notified magellan personnel in the area who subsequently conducted an investigation and discovered a pinhole leak in a girth weld. The line was repaired by installing a type b full encirclement sleeve and the pipe repair was coated. Approximately 600 cubic yards of impacted soil was remediated in accordance with state and company standards.
Detailed record list
Report Received Date
2012-09-28 00:00:00
Iyear
2012
Report Number
20120279
Supplemental Number
19205
Report Type
Supplemental Final
Operator Id
Name
Magellan Ammonia Pipeline, L.p.
Operator Street Address
One Williams Center, Otc-9 P.o. Box 22186
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2012-09-09 07:35:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
54.65
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2012-09-09 07:35:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-09-09 07:35:00
Restart Datetime
2012-09-10 14:50:00
On Site Datetime
2012-09-09 13:00:00
Nrc Rpt Datetime
2012-09-09 08:52:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Pipe Fac Name
Early To Garner Line Ssegment
Segment Name
Line Segment #504
Onshore State Abbreviation
Ia
Onshore Postal Code
50574
Onshore City Name
Pocahontas
Onshore County Name
Pocahontas
Designated Location
Milepost/valve Station
Designated Name
92.8
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
6.625
Pipe Wall Thickness
0.156
Pipe Smys
46000
Pipe Specification
Api 5lx 46
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Lone Star Steel
Pipe Coating Type
Cold Applied Tape
Weld Subtype
Pipe Girth Weld
Installation Year
1968
Manufactured Year
1968
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
2700
Est Cost Gas Released
4408
Est Cost Prop Damage
5000
Est Cost Emergency
5086
Est Cost Environmental
25000
Est Cost Other
300
Est Cost Other Details
Plastic Sheeting, Sandblasting Sand
Prpty
42494
Accident Psig
421
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
157603
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Incompat Commod Ind
Yes
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The system was operating normally up to and at the time the event was initially reported, with no alarms or other indications reported by scada or cpm, and it was determined that neither the control room nor the controller operating the line caused or contributed to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Pinhole In Girth Weld
Pwf Additional Other Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2007
Geometry Recent Year
2007
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2011
Hydrtst Most Rcnt Pressure
1965
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7246
Prepared Date
2014-04-03 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
Aerial patrol pilot spotted a small area of distressed vegetation in a cultivated field and notified magellan personnel in the area who subsequently conducted an investigation and discovered a pinhole leak in a girth weld. The line was repaired by installing a type b full encirclement sleeve and the pipe repair was coated. Approximately 600 cubic yards of impacted soil was remediated in accordance with state and company standards.
Report Received Date 2012-09-28 00:00:00
Iyear 2012
Report Number 20120279
Supplemental Number 19205
Report Type Supplemental Final
Operator Id 12105 PHMSA Enforcement
Name Magellan Ammonia Pipeline, L.p.
Operator Street Address One Williams Center, Otc-9 P.o. Box 22186
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Local Datetime 2012-09-09 07:35:00
Location Latitude 42.72143 Google Maps OpenStreetMap
Location Longitude -94.60402 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Anhydrous Ammonia
Unintentional Release Bbls 54.65
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2012-09-09 07:35:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-09-09 07:35:00
Restart Datetime 2012-09-10 14:50:00
On Site Datetime 2012-09-09 13:00:00
Nrc Rpt Datetime 2012-09-09 08:52:00
Nrc Rpt Num 1023811 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Pipe Fac Name Early To Garner Line Ssegment
Segment Name Line Segment #504
Onshore State Abbreviation Ia
Onshore Postal Code 50574
Onshore City Name Pocahontas
Onshore County Name Pocahontas
Designated Location Milepost/valve Station
Designated Name 92.8
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Pipe Diameter 6.625
Pipe Wall Thickness 0.156
Pipe Smys 46000
Pipe Specification Api 5lx 46
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Lone Star Steel
Pipe Coating Type Cold Applied Tape
Weld Subtype Pipe Girth Weld
Installation Year 1968
Manufactured Year 1968
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 2700
Est Cost Gas Released 4408
Est Cost Prop Damage 5000
Est Cost Emergency 5086
Est Cost Environmental 25000
Est Cost Other 300
Est Cost Other Details Plastic Sheeting, Sandblasting Sand
Prpty 42494
Accident Psig 421
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 157603
Internal Inspection Ind Yes
Operation Complications Ind Yes
Incompat Commod Ind Yes
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The system was operating normally up to and at the time the event was initially reported, with no alarms or other indications reported by scada or cpm, and it was determined that neither the control room nor the controller operating the line caused or contributed to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details Pinhole In Girth Weld
Pwf Additional Other Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2007
Geometry Recent Year 2007
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2011
Hydrtst Most Rcnt Pressure 1965
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name K****** L* L*******
Preparer Title Sr. Compliance Coordinator
Preparer Email K***********@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7246
Prepared Date 2014-04-03 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Sr. Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative Aerial patrol pilot spotted a small area of distressed vegetation in a cultivated field and notified magellan personnel in the area who subsequently conducted an investigation and discovered a pinhole leak in a girth weld. The line was repaired by installing a type b full encirclement sleeve and the pipe repair was coated. Approximately 600 cubic yards of impacted soil was remediated in accordance with state and company standards.

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