HL incident on 2012-08-23 — OH

Operator
Marathon Pipe Line Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$89,878
Incident datetime
2012-08-23 15:20
Report number
Location
OH
Narrative
During routine maintenance at effingham, area personnel were not able to obtain the proper isolation by just closing the station valves. As a result, they had the mainline shut down and closed the upstream and downstream block valves. With the change in energy isolation plans, the area personnel failed to recognize and lock out the sump. Shortly after the upstream and downstream block valves were closed, the effingham sump kicked on (14:47) causing the pressure on the mainline between the two block valves to increase to 1500+ psig, exceeding 110% of mop. At 15:20, field personnel discovered that the resulting pressure increase caused the insulating gasket on the downstream side of valve bv1 to rupture, releasing approximately 7 gallons of crude oil to the environment. The line was excavated, all contaminated soil was removed, and the insulating gasket was replaced with a flexitallic gasket and new studs.
Detailed record list
Report Received Date
2012-09-12 00:00:00
Iyear
2012
Report Number
20120260
Supplemental Number
17973
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2012-08-23 14:47:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.2
Intentional Release Bbls
0
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2012-08-23 15:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Already Down For Work.
On Site Datetime
2012-08-23 15:20:00
Nrc Rpt Datetime
2012-08-24 00:25:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Patoka - Martinsville System
Segment Name
Effingham Station
Onshore State Abbreviation
Il
Onshore Postal Code
62401
Onshore City Name
Effingham
Onshore County Name
Effingham
Designated Location
Survey Station No.
Designated Name
1950+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
30
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Insulating Gasket On Flange
Material Involved
Material Other Than Carbon Steel
Material Details
Resin
Release Type
Leak
Leak Type
Other
Leak Type Other
Gasket Rupture
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
89878
Est Cost Emergency
15504
Est Cost Environmental
0
Est Cost Other
0
Prpty
105402
Accident Psig
1500
Mop Psig
1044
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Invest Maint Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Pipeline Or Equipment Overpressured
Operation Type
Pipeline Or Equipment Overpressured
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
R**** S********
Preparer Title
Hes Professional
Preparer Email
R**********@m****************.com
Preparer Telephone
4194212121
Prepared Date
2013-04-29 00:00:00
Authorizer Name
R****** B*****
Authorizer Telephone
4194212121
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
During routine maintenance at effingham, area personnel were not able to obtain the proper isolation by just closing the station valves. As a result, they had the mainline shut down and closed the upstream and downstream block valves. With the change in energy isolation plans, the area personnel failed to recognize and lock out the sump. Shortly after the upstream and downstream block valves were closed, the effingham sump kicked on (14:47) causing the pressure on the mainline between the two block valves to increase to 1500+ psig, exceeding 110% of mop. At 15:20, field personnel discovered that the resulting pressure increase caused the insulating gasket on the downstream side of valve bv1 to rupture, releasing approximately 7 gallons of crude oil to the environment. The line was excavated, all contaminated soil was removed, and the insulating gasket was replaced with a flexitallic gasket and new studs.
Report Received Date 2012-09-12 00:00:00
Iyear 2012
Report Number 20120260
Supplemental Number 17973
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2012-08-23 14:47:00
Location Latitude 39.060075 Google Maps OpenStreetMap
Location Longitude -88.495556 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.2
Intentional Release Bbls 0
Recovered Bbls 0.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2012-08-23 15:20:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Already Down For Work.
On Site Datetime 2012-08-23 15:20:00
Nrc Rpt Datetime 2012-08-24 00:25:00
Nrc Rpt Num 1022043 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Patoka - Martinsville System
Segment Name Effingham Station
Onshore State Abbreviation Il
Onshore Postal Code 62401
Onshore City Name Effingham
Onshore County Name Effingham
Designated Location Survey Station No.
Designated Name 1950+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 30
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Insulating Gasket On Flange
Material Involved Material Other Than Carbon Steel
Material Details Resin
Release Type Leak
Leak Type Other
Leak Type Other Gasket Rupture
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 89878
Est Cost Emergency 15504
Est Cost Environmental 0
Est Cost Other 0
Prpty 105402
Accident Psig 1500
Mop Psig 1044
Accident Pressure Pressure Exceeded 110% Of Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Invest Maint Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Pipeline Or Equipment Overpressured
Operation Type Pipeline Or Equipment Overpressured
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name R**** S********
Preparer Title Hes Professional
Preparer Email R**********@m****************.com
Preparer Telephone 4194212121
Prepared Date 2013-04-29 00:00:00
Authorizer Name R****** B*****
Authorizer Telephone 4194212121
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative During routine maintenance at effingham, area personnel were not able to obtain the proper isolation by just closing the station valves. As a result, they had the mainline shut down and closed the upstream and downstream block valves. With the change in energy isolation plans, the area personnel failed to recognize and lock out the sump. Shortly after the upstream and downstream block valves were closed, the effingham sump kicked on (14:47) causing the pressure on the mainline between the two block valves to increase to 1500+ psig, exceeding 110% of mop. At 15:20, field personnel discovered that the resulting pressure increase caused the insulating gasket on the downstream side of valve bv1 to rupture, releasing approximately 7 gallons of crude oil to the environment. The line was excavated, all contaminated soil was removed, and the insulating gasket was replaced with a flexitallic gasket and new studs.

All rights reserved. Copyright © by ClearPHMSA