HL incident on 2012-07-23 — TX

Operator
The Dow Chemical Company
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,000,000
Incident datetime
2012-07-23 20:00
Report number
Location
TX
Narrative
On july 23, 2012 at 20:00 hours the dow chemical company emergency services received a telephone report from the public of a strange odor. The report stated the odor was near highway 332 and the dow chemical company levee. Emergency services personnel investigated the report and found a wet spot on the ground near several pipelines. Emergency services contacted the dow chemical company site pipeline operations department. Site pipeline operations personnel responded and arrived at the odor location around 20:10 hours. Samples of the source of the odor were taken and analyzed. The material was identified as naphtha. Investigation showed that the only naphtha line in the area was dpl-145. The dpl-145 control center was contacted. Investigation showed that dpl-145 had experienced a rapid pressure drop. Site pipeline operations personnel proceeded to contain the leak by blocking in additional valves on dpl-145. Investigation showed that dpl-145 was already out of service and was in the process of an evaluation for maintenance. The pipeline was full of liquid but was not flowing. Currently remediation operations are underway. The pipeline is isolated, de-pressured and in the process of being cleared. Additional supplemental information as of 11/5/12: pipeline remains out of service. The cause of the leak was internal corrosion which failed due to thermal expansion. Temporary clamps have been installed at leak site. Pipeline has not been cut open as of yet. Pipeline is awaiting final disposition. We will both repair and re-commission or abandon the pipeline based on a business and financial analysis. Pipeline is out of service, cleared or product but not clean. It is air gapped on both ends. This pipeline will potentially be out of service for the next 3 years.
Detailed record list
Report Received Date
2012-08-23 00:00:00
Iyear
2012
Report Number
20120245
Supplemental Number
19354
Report Type
Supplemental Final
Operator Id
Name
The Dow Chemical Company
Operator Street Address
6723 E. Hwy 332 Bldg Bm-59
Operator City Name
Freeport
Operator State Abbreviation
TX
Operator Postal Code
77541
Local Datetime
2012-07-23 20:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Naphtha
Unintentional Release Bbls
132
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2012-07-23 20:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Already Out Of Service
On Site Datetime
2012-07-23 20:10:00
Nrc Rpt Datetime
2012-07-24 04:23:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
The Dow Chemical Company
Segment Name
Dpl-145
Onshore State Abbreviation
Tx
Onshore Postal Code
77541
Onshore City Name
Freeport
Onshore County Name
Brazoria
Designated Location
Survey Station No.
Designated Name
T-T135
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
34
Pipe Wall Thickness
0.329
Pipe Smys
60000
Pipe Specification
Api 5lx60
Pipe Seam Type
Dsaw
Pipe Manufacturer
U.s. Steel
Pipe Coating Type
Cold Applied Tape
Installation Year
1978
Manufactured Year
1977
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Width
1
Rupture Length
121
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
13980
Est Cost Prop Damage
2000000
Est Cost Emergency
200000
Est Cost Environmental
4000000
Est Cost Other
0
Prpty
6213980
Accident Psig
250
Mop Psig
605
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
32031
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Excessive Debris Ind
Yes
Low Flow Ind
Yes
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline was already out of service and no controller operations were necessary.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Corrosive Commodity Ind
Yes
Int Water Acid Ind
Yes
Int Other Basis Ind
Yes
Int Corrosion Basis Details
Process Knowledge
Int Other Loc Ind
Yes
Corrosion Location Details
Longitudinal Area Along The 4 O'clock Position And Occured In Lowest Elevation Of Pipeline.
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
No
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Axial Recent Year
2009
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1991
Hydrtst Most Rcnt Pressure
1050
Direct Asmnt Conducted
No
Non Destructive Exam Ind
Yes
Exm Wave Ultrasonic Rcnt Year
2012
Exm Handl Ultrasonic Rcnt Year
2012
Exm Wave Ultrasonic Rcnt Ind
Yes
Exm Handl Ultrasonic Rcnt Ind
Yes
Preparer Name
S****** N*********
Preparer Title
Compliance Leader
Preparer Email
S***********@d**.com
Preparer Telephone
979-238-5964
Preparer Fax
979-238-0911
Prepared Date
2014-05-01 00:00:00
Authorizer Name
R***** C* T*****
Authorizer Telephone
979-238-4770
Authorizer Title
Process Leader
Authorizer Email
R*******@d**.com
Narrative
On july 23, 2012 at 20:00 hours the dow chemical company emergency services received a telephone report from the public of a strange odor. The report stated the odor was near highway 332 and the dow chemical company levee. Emergency services personnel investigated the report and found a wet spot on the ground near several pipelines. Emergency services contacted the dow chemical company site pipeline operations department. Site pipeline operations personnel responded and arrived at the odor location around 20:10 hours. Samples of the source of the odor were taken and analyzed. The material was identified as naphtha. Investigation showed that the only naphtha line in the area was dpl-145. The dpl-145 control center was contacted. Investigation showed that dpl-145 had experienced a rapid pressure drop. Site pipeline operations personnel proceeded to contain the leak by blocking in additional valves on dpl-145. Investigation showed that dpl-145 was already out of service and was in the process of an evaluation for maintenance. The pipeline was full of liquid but was not flowing. Currently remediation operations are underway. The pipeline is isolated, de-pressured and in the process of being cleared. Additional supplemental information as of 11/5/12: pipeline remains out of service. The cause of the leak was internal corrosion which failed due to thermal expansion. Temporary clamps have been installed at leak site. Pipeline has not been cut open as of yet. Pipeline is awaiting final disposition. We will both repair and re-commission or abandon the pipeline based on a business and financial analysis. Pipeline is out of service, cleared or product but not clean. It is air gapped on both ends. This pipeline will potentially be out of service for the next 3 years.
Report Received Date 2012-08-23 00:00:00
Iyear 2012
Report Number 20120245
Supplemental Number 19354
Report Type Supplemental Final
Operator Id 30959 PHMSA Enforcement
Name The Dow Chemical Company
Operator Street Address 6723 E. Hwy 332 Bldg Bm-59
Operator City Name Freeport
Operator State Abbreviation TX
Operator Postal Code 77541
Local Datetime 2012-07-23 20:00:00
Location Latitude 28.9598 Google Maps OpenStreetMap
Location Longitude -95.31151 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Other
Commodity Details Naphtha
Unintentional Release Bbls 132
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2012-07-23 20:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Already Out Of Service
On Site Datetime 2012-07-23 20:10:00
Nrc Rpt Datetime 2012-07-24 04:23:00
Nrc Rpt Num 1018894 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name The Dow Chemical Company
Segment Name Dpl-145
Onshore State Abbreviation Tx
Onshore Postal Code 77541
Onshore City Name Freeport
Onshore County Name Brazoria
Designated Location Survey Station No.
Designated Name T-T135
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 34
Pipe Wall Thickness 0.329
Pipe Smys 60000
Pipe Specification Api 5lx60
Pipe Seam Type Dsaw
Pipe Manufacturer U.s. Steel
Pipe Coating Type Cold Applied Tape
Installation Year 1978
Manufactured Year 1977
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Width 1
Rupture Length 121
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 13980
Est Cost Prop Damage 2000000
Est Cost Emergency 200000
Est Cost Environmental 4000000
Est Cost Other 0
Prpty 6213980
Accident Psig 250
Mop Psig 605
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 32031
Internal Inspection Ind Yes
Operation Complications Ind Yes
Excessive Debris Ind Yes
Low Flow Ind Yes
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pipeline was already out of service and no controller operations were necessary.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Not Cut Open
Int Corrosive Commodity Ind Yes
Int Water Acid Ind Yes
Int Other Basis Ind Yes
Int Corrosion Basis Details Process Knowledge
Int Other Loc Ind Yes
Corrosion Location Details Longitudinal Area Along The 4 O'clock Position And Occured In Lowest Elevation Of Pipeline.
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons No
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Axial Recent Year 2009
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1991
Hydrtst Most Rcnt Pressure 1050
Direct Asmnt Conducted No
Non Destructive Exam Ind Yes
Exm Wave Ultrasonic Rcnt Year 2012
Exm Handl Ultrasonic Rcnt Year 2012
Exm Wave Ultrasonic Rcnt Ind Yes
Exm Handl Ultrasonic Rcnt Ind Yes
Preparer Name S****** N*********
Preparer Title Compliance Leader
Preparer Email S***********@d**.com
Preparer Telephone 979-238-5964
Preparer Fax 979-238-0911
Prepared Date 2014-05-01 00:00:00
Authorizer Name R***** C* T*****
Authorizer Telephone 979-238-4770
Authorizer Title Process Leader
Authorizer Email R*******@d**.com
Narrative On july 23, 2012 at 20:00 hours the dow chemical company emergency services received a telephone report from the public of a strange odor. The report stated the odor was near highway 332 and the dow chemical company levee. Emergency services personnel investigated the report and found a wet spot on the ground near several pipelines. Emergency services contacted the dow chemical company site pipeline operations department. Site pipeline operations personnel responded and arrived at the odor location around 20:10 hours. Samples of the source of the odor were taken and analyzed. The material was identified as naphtha. Investigation showed that the only naphtha line in the area was dpl-145. The dpl-145 control center was contacted. Investigation showed that dpl-145 had experienced a rapid pressure drop. Site pipeline operations personnel proceeded to contain the leak by blocking in additional valves on dpl-145. Investigation showed that dpl-145 was already out of service and was in the process of an evaluation for maintenance. The pipeline was full of liquid but was not flowing. Currently remediation operations are underway. The pipeline is isolated, de-pressured and in the process of being cleared. Additional supplemental information as of 11/5/12: pipeline remains out of service. The cause of the leak was internal corrosion which failed due to thermal expansion. Temporary clamps have been installed at leak site. Pipeline has not been cut open as of yet. Pipeline is awaiting final disposition. We will both repair and re-commission or abandon the pipeline based on a business and financial analysis. Pipeline is out of service, cleared or product but not clean. It is air gapped on both ends. This pipeline will potentially be out of service for the next 3 years.

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