HL incident on 2012-07-23 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2012-07-23 10:00
Report number
Location
GA
Narrative
On july 23, 2012 at 10:00 (local time), a colonial technician arrived at staten island jct for maintenance activities and discovered product on the ground. At 10:02 immediate notifications were made to the associate director of operations, who made the required internal and agency notifications. The pipeline was shut down and isolated. Response personnel removed the product, excavated the contaminated soil and placed on plastic, excavated pot holes to determine the extent of the product spill and installed protective down gradient barrier trenches with absorbent boom. The check valve was repaired with a new gasket and the line returned to normal operations. On july 30, 2012 the cost related to the leak were estimated to exceed $50,000, and accordingly nrc notification number 1019460 was made.
Detailed record list
Report Received Date
2012-08-14 00:00:00
Iyear
2012
Report Number
20120236
Supplemental Number
17079
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1185 Sanctuary Parkway, Suite 100
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009-4765
Local Datetime
2012-07-23 10:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
27.4
Intentional Release Bbls
0
Recovered Bbls
27.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-07-23 10:02:00
Restart Datetime
2012-07-23 18:19:00
Nrc Rpt Datetime
2012-07-30 18:04:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Pipe Fac Name
Colonial/staten Island Junction
Segment Name
Linden To Imtt
Onshore State Abbreviation
Ny
Onshore Postal Code
10301
Onshore City Name
Staten Island
Onshore County Name
Richmond
Designated Location
Survey Station No.
Designated Name
4010
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Transition Area
Incident Area Subtype
Soil/air Interface
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
1963
Material Involved
Material Other Than Carbon Steel
Material Details
Flexitallic Gasket
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
3900
Est Cost Prop Damage
10000
Est Cost Emergency
40000
Est Cost Environmental
8500
Est Cost Other
0
Prpty
62400
Accident Psig
330
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
40
Internal Inspection Ind
No
Other Restrictions Ind
Yes
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Line Configuration Not Piggable
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller(s) or control room issues were not the cause of or a contributing factor to the accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Eq Additional Other Ind
Yes
Eq Additional Other Details
Wear
Preparer Name
A* M* T*****
Preparer Title
Regulatory Manager
Preparer Email
A******@c******.com
Preparer Telephone
6787622872
Preparer Fax
6787622315
Prepared Date
2012-12-07 00:00:00
Authorizer Name
A* M* T*****
Authorizer Telephone
6787622872
Authorizer Title
Regulatory Manager
Authorizer Email
A******@c******.com
Narrative
On july 23, 2012 at 10:00 (local time), a colonial technician arrived at staten island jct for maintenance activities and discovered product on the ground. At 10:02 immediate notifications were made to the associate director of operations, who made the required internal and agency notifications. The pipeline was shut down and isolated. Response personnel removed the product, excavated the contaminated soil and placed on plastic, excavated pot holes to determine the extent of the product spill and installed protective down gradient barrier trenches with absorbent boom. The check valve was repaired with a new gasket and the line returned to normal operations. On july 30, 2012 the cost related to the leak were estimated to exceed $50,000, and accordingly nrc notification number 1019460 was made.
Report Received Date 2012-08-14 00:00:00
Iyear 2012
Report Number 20120236
Supplemental Number 17079
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1185 Sanctuary Parkway, Suite 100
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009-4765
Local Datetime 2012-07-23 10:00:00
Location Latitude 40.6246 Google Maps OpenStreetMap
Location Longitude -74.19254 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 27.4
Intentional Release Bbls 0
Recovered Bbls 27.4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-07-23 10:02:00
Restart Datetime 2012-07-23 18:19:00
Nrc Rpt Datetime 2012-07-30 18:04:00
Nrc Rpt Num 1019460 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Pipe Fac Name Colonial/staten Island Junction
Segment Name Linden To Imtt
Onshore State Abbreviation Ny
Onshore Postal Code 10301
Onshore City Name Staten Island
Onshore County Name Richmond
Designated Location Survey Station No.
Designated Name 4010
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Transition Area
Incident Area Subtype Soil/air Interface
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 1963
Material Involved Material Other Than Carbon Steel
Material Details Flexitallic Gasket
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 3900
Est Cost Prop Damage 10000
Est Cost Emergency 40000
Est Cost Environmental 8500
Est Cost Other 0
Prpty 62400
Accident Psig 330
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 40
Internal Inspection Ind No
Other Restrictions Ind Yes
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Line Configuration Not Piggable
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller(s) or control room issues were not the cause of or a contributing factor to the accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Eq Additional Other Ind Yes
Eq Additional Other Details Wear
Preparer Name A* M* T*****
Preparer Title Regulatory Manager
Preparer Email A******@c******.com
Preparer Telephone 6787622872
Preparer Fax 6787622315
Prepared Date 2012-12-07 00:00:00
Authorizer Name A* M* T*****
Authorizer Telephone 6787622872
Authorizer Title Regulatory Manager
Authorizer Email A******@c******.com
Narrative On july 23, 2012 at 10:00 (local time), a colonial technician arrived at staten island jct for maintenance activities and discovered product on the ground. At 10:02 immediate notifications were made to the associate director of operations, who made the required internal and agency notifications. The pipeline was shut down and isolated. Response personnel removed the product, excavated the contaminated soil and placed on plastic, excavated pot holes to determine the extent of the product spill and installed protective down gradient barrier trenches with absorbent boom. The check valve was repaired with a new gasket and the line returned to normal operations. On july 30, 2012 the cost related to the leak were estimated to exceed $50,000, and accordingly nrc notification number 1019460 was made.

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