HL incident on 2012-07-20 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,000
Incident datetime
2012-07-20 04:00
Report number
Location
TX
Narrative
0400 hobbs station operator recognizes small product leak venting from sk-hb blue filter inlet valve, an 8" grove. Operator monitored the condition and remained constant. 0615 supervision observes leak and monitors, personnel remain attentive to condition and had made determination that the stem o-ring / packing was the source. Ethane / propane ngl is the product. 0800 operations personnel manipulate valve in an effort to reduce the product venting. Venting did not slow down and notification was made to pl control to shut the pipeline down. 1600 pipeline was restarted with the valve repaired.
Detailed record list
Report Received Date
2012-08-09 00:00:00
Iyear
2012
Report Number
20120231
Supplemental Number
16817
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-07-20 04:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
6.3
Intentional Release Bbls
6
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2012-07-20 04:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-07-20 08:00:00
Restart Datetime
2012-07-20 16:00:00
On Site Datetime
2012-07-20 04:00:00
Nrc Rpt Datetime
2012-07-20 09:24:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Hobbs Station
Segment Name
South Leg Pid 617
Onshore State Abbreviation
Tx
Onshore Postal Code
79360
Onshore City Name
Seminole
Onshore County Name
Gaines
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Weephole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
245
Est Cost Prop Damage
3000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
3245
Accident Psig
700
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
100
Internal Inspection Ind
No
Diameter Change Ind
Yes
Tight Mitered Ind
Yes
Other Restrictions Ind
Yes
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Valve stem o-ring failed and was replaced the same day.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Wear
Preparer Name
N*** V* T*****
Preparer Title
Pipeline Compliance Specialist
Preparer Email
N*******@e****.com
Preparer Telephone
713-381-2493
Prepared Date
2012-08-09 00:00:00
Authorizer Name
N*** V* T*****
Authorizer Telephone
713-381-2493
Authorizer Title
Pipeline Compliance Specialist
Authorizer Email
N*******@e****.com
Narrative
0400 hobbs station operator recognizes small product leak venting from sk-hb blue filter inlet valve, an 8" grove. Operator monitored the condition and remained constant. 0615 supervision observes leak and monitors, personnel remain attentive to condition and had made determination that the stem o-ring / packing was the source. Ethane / propane ngl is the product. 0800 operations personnel manipulate valve in an effort to reduce the product venting. Venting did not slow down and notification was made to pl control to shut the pipeline down. 1600 pipeline was restarted with the valve repaired.
Report Received Date 2012-08-09 00:00:00
Iyear 2012
Report Number 20120231
Supplemental Number 16817
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2012-07-20 04:00:00
Location Latitude 32.779328 Google Maps OpenStreetMap
Location Longitude -102.950633 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 6.3
Intentional Release Bbls 6
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2012-07-20 04:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-07-20 08:00:00
Restart Datetime 2012-07-20 16:00:00
On Site Datetime 2012-07-20 04:00:00
Nrc Rpt Datetime 2012-07-20 09:24:00
Nrc Rpt Num 1018373 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Hobbs Station
Segment Name South Leg Pid 617
Onshore State Abbreviation Tx
Onshore Postal Code 79360
Onshore City Name Seminole
Onshore County Name Gaines
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Weephole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 245
Est Cost Prop Damage 3000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 3245
Accident Psig 700
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 100
Internal Inspection Ind No
Diameter Change Ind Yes
Tight Mitered Ind Yes
Other Restrictions Ind Yes
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Valve stem o-ring failed and was replaced the same day.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Wear
Preparer Name N*** V* T*****
Preparer Title Pipeline Compliance Specialist
Preparer Email N*******@e****.com
Preparer Telephone 713-381-2493
Prepared Date 2012-08-09 00:00:00
Authorizer Name N*** V* T*****
Authorizer Telephone 713-381-2493
Authorizer Title Pipeline Compliance Specialist
Authorizer Email N*******@e****.com
Narrative 0400 hobbs station operator recognizes small product leak venting from sk-hb blue filter inlet valve, an 8" grove. Operator monitored the condition and remained constant. 0615 supervision observes leak and monitors, personnel remain attentive to condition and had made determination that the stem o-ring / packing was the source. Ethane / propane ngl is the product. 0800 operations personnel manipulate valve in an effort to reduce the product venting. Venting did not slow down and notification was made to pl control to shut the pipeline down. 1600 pipeline was restarted with the valve repaired.

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