HL incident on 2012-06-21 — KS

Operator
Nustar Pipeline Operating Partnership L.p.
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2012-06-21 10:00
Report number
Location
KS
Narrative
On june 9, 2012 a landowner notified nustar of odors coming from his irrigation well. Nustar pipeline runs east/west approximately 45 feet north of this well. The line has been shut in since march 2012 and scada confirms pressures holding at 465 psi. On june 13 a 45 foot section of the pipeline was excavated with no signs of hydrocarbon in the excavation nor a leak point. It was speculated that someone could have sabotaged the well by dumping gasoline down his unlocked well due to landowner comment regarding recent domestic event. On june 18 nustar evacuated a 5000 foot section of pipe. On june 19-21, nustar pressure tested at 1800 psi with water the 5000 foot section which lost pressure of 1-2 psi every 45 seconds, but stabilized at 565 psi. On june 24 praxair leak detection services applied their process to detect a leak and was unsuccessful. On june 26 the section was divided into 2-2000 foot sections and both sections were pressure tested on june 27. The segment to the west did not hold pressure. On june 29 a 250 foot section was isolated and pressure tested and lost 45 psi per minute. On july 5-6, the 250 foot segment was excavated and a small hole was found. No other failure points were found. The failure point will be cut out and sent to keifner for metallurgical analysis. On 8/30/12 a supplemental report was submitted due to the increase cost of public and non-operator private property damage exceeding $20,000 of original estimate. Still waiting on a report from keifner. Kiefner report finalized on october 30, 2012 indicating the cause of leak was selective seam corrosion which occurred at a pre-existing lack-of-fusion defect within the erw seam. Total soil excavated was 16 cubic yards which was landfarmed at a kdhe approved site at nustar el dorado station. 6/19/15 - this will be the final report. This site has gone to long term remediation and product recovery has diminished to a point of insignificance. Total recovered is 5.69 barrels.
Detailed record list
Report Received Date
2012-07-10 00:00:00
Iyear
2012
Report Number
20120210
Supplemental Number
20535
Report Type
Supplemental Final
Operator Id
Name
Nustar Pipeline Operating Partnership L.p.
Operator Street Address
7340 W. 21st Street North
Operator City Name
Wichita
Operator State Abbreviation
KS
Operator Postal Code
67205
Local Datetime
2012-06-21 10:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
5.69
Intentional Release Bbls
0
Recovered Bbls
5.69
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Static Shut-In Test Or Other Pressure Or Leak Test
Incident Identified Datetime
2012-06-21 10:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-06-21 10:00:00
Restart Datetime
2012-08-31 06:00:00
On Site Datetime
2012-06-21 10:00:00
Nrc Rpt Datetime
2012-07-07 10:53:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Wichita To Augusta 8 Inch
Segment Name
21st Street Jct To Augusta
Onshore State Abbreviation
Ks
Onshore Postal Code
67002
Onshore City Name
Andover
Onshore County Name
Butler
Designated Location
Milepost/valve Station
Designated Name
10.34
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
96
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Uncased
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Pipe Wall Thickness
0.25
Pipe Smys
35000
Pipe Specification
Api 5ls-B
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1954
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
2.3
Rel Water Name
First Water Bearing Zone
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
91411
Est Cost Gas Released
250
Est Cost Prop Damage
5000
Est Cost Emergency
50000
Est Cost Environmental
5000
Est Cost Other
0
Prpty
151661
Accident Psig
465
Mop Psig
1349
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
56496
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
At the time of notification by public the line was shut in and holding pressure at 465 psi. On june 21, 2012 a pressure test inidcated a pressure loss of 1-2 psi every 45 seconds.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
General Corrosion
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Selective Seam Corrosion
Int Metallurgical Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
Seam
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2010
Circ Wave Recent Year
2007
Geometry Recent Year
2010
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr
2009
Non Destructive Exam Ind
No
Preparer Name
D***** J* T******
Preparer Title
Director - Hse
Preparer Email
D**********@n***********.com
Preparer Telephone
316-721-7056
Preparer Fax
316-773-9001
Prepared Date
2015-06-19 00:00:00
Authorizer Name
B*** F******
Authorizer Telephone
316-721-7066
Authorizer Title
General Manager
Authorizer Email
B***********@n***********.com
Narrative
On june 9, 2012 a landowner notified nustar of odors coming from his irrigation well. Nustar pipeline runs east/west approximately 45 feet north of this well. The line has been shut in since march 2012 and scada confirms pressures holding at 465 psi. On june 13 a 45 foot section of the pipeline was excavated with no signs of hydrocarbon in the excavation nor a leak point. It was speculated that someone could have sabotaged the well by dumping gasoline down his unlocked well due to landowner comment regarding recent domestic event. On june 18 nustar evacuated a 5000 foot section of pipe. On june 19-21, nustar pressure tested at 1800 psi with water the 5000 foot section which lost pressure of 1-2 psi every 45 seconds, but stabilized at 565 psi. On june 24 praxair leak detection services applied their process to detect a leak and was unsuccessful. On june 26 the section was divided into 2-2000 foot sections and both sections were pressure tested on june 27. The segment to the west did not hold pressure. On june 29 a 250 foot section was isolated and pressure tested and lost 45 psi per minute. On july 5-6, the 250 foot segment was excavated and a small hole was found. No other failure points were found. The failure point will be cut out and sent to keifner for metallurgical analysis. On 8/30/12 a supplemental report was submitted due to the increase cost of public and non-operator private property damage exceeding $20,000 of original estimate. Still waiting on a report from keifner. Kiefner report finalized on october 30, 2012 indicating the cause of leak was selective seam corrosion which occurred at a pre-existing lack-of-fusion defect within the erw seam. Total soil excavated was 16 cubic yards which was landfarmed at a kdhe approved site at nustar el dorado station. 6/19/15 - this will be the final report. This site has gone to long term remediation and product recovery has diminished to a point of insignificance. Total recovered is 5.69 barrels.
Report Received Date 2012-07-10 00:00:00
Iyear 2012
Report Number 20120210
Supplemental Number 20535
Report Type Supplemental Final
Operator Id 10012 PHMSA Enforcement
Name Nustar Pipeline Operating Partnership L.p.
Operator Street Address 7340 W. 21st Street North
Operator City Name Wichita
Operator State Abbreviation KS
Operator Postal Code 67205
Local Datetime 2012-06-21 10:00:00
Location Latitude 37.721901 Google Maps OpenStreetMap
Location Longitude -97.147138 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 5.69
Intentional Release Bbls 0
Recovered Bbls 5.69
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Static Shut-In Test Or Other Pressure Or Leak Test
Incident Identified Datetime 2012-06-21 10:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-06-21 10:00:00
Restart Datetime 2012-08-31 06:00:00
On Site Datetime 2012-06-21 10:00:00
Nrc Rpt Datetime 2012-07-07 10:53:00
Nrc Rpt Num 1016989 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Wichita To Augusta 8 Inch
Segment Name 21st Street Jct To Augusta
Onshore State Abbreviation Ks
Onshore Postal Code 67002
Onshore City Name Andover
Onshore County Name Butler
Designated Location Milepost/valve Station
Designated Name 10.34
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 96
Crossing Yes
Road Crossing Ind Yes
Road Type Uncased
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8.625
Pipe Wall Thickness 0.25
Pipe Smys 35000
Pipe Specification Api 5ls-B
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1954
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 2.3
Rel Water Name First Water Bearing Zone
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 91411
Est Cost Gas Released 250
Est Cost Prop Damage 5000
Est Cost Emergency 50000
Est Cost Environmental 5000
Est Cost Other 0
Prpty 151661
Accident Psig 465
Mop Psig 1349
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 56496
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details At the time of notification by public the line was shut in and holding pressure at 465 psi. On june 21, 2012 a pressure test inidcated a pressure loss of 1-2 psi every 45 seconds.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results General Corrosion
Int Other Corrosion Ind Yes
Int Corrosion Type Details Selective Seam Corrosion
Int Metallurgical Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details Seam
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Yes
Corrosion Coupons Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2010
Circ Wave Recent Year 2007
Geometry Recent Year 2010
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted Yes, But The Point Of The Accident Was Not Identified As A Dig Site
Direct Asmnt Pnt Not Idntf Yr 2009
Non Destructive Exam Ind No
Preparer Name D***** J* T******
Preparer Title Director - Hse
Preparer Email D**********@n***********.com
Preparer Telephone 316-721-7056
Preparer Fax 316-773-9001
Prepared Date 2015-06-19 00:00:00
Authorizer Name B*** F******
Authorizer Telephone 316-721-7066
Authorizer Title General Manager
Authorizer Email B***********@n***********.com
Narrative On june 9, 2012 a landowner notified nustar of odors coming from his irrigation well. Nustar pipeline runs east/west approximately 45 feet north of this well. The line has been shut in since march 2012 and scada confirms pressures holding at 465 psi. On june 13 a 45 foot section of the pipeline was excavated with no signs of hydrocarbon in the excavation nor a leak point. It was speculated that someone could have sabotaged the well by dumping gasoline down his unlocked well due to landowner comment regarding recent domestic event. On june 18 nustar evacuated a 5000 foot section of pipe. On june 19-21, nustar pressure tested at 1800 psi with water the 5000 foot section which lost pressure of 1-2 psi every 45 seconds, but stabilized at 565 psi. On june 24 praxair leak detection services applied their process to detect a leak and was unsuccessful. On june 26 the section was divided into 2-2000 foot sections and both sections were pressure tested on june 27. The segment to the west did not hold pressure. On june 29 a 250 foot section was isolated and pressure tested and lost 45 psi per minute. On july 5-6, the 250 foot segment was excavated and a small hole was found. No other failure points were found. The failure point will be cut out and sent to keifner for metallurgical analysis. On 8/30/12 a supplemental report was submitted due to the increase cost of public and non-operator private property damage exceeding $20,000 of original estimate. Still waiting on a report from keifner. Kiefner report finalized on october 30, 2012 indicating the cause of leak was selective seam corrosion which occurred at a pre-existing lack-of-fusion defect within the erw seam. Total soil excavated was 16 cubic yards which was landfarmed at a kdhe approved site at nustar el dorado station. 6/19/15 - this will be the final report. This site has gone to long term remediation and product recovery has diminished to a point of insignificance. Total recovered is 5.69 barrels.

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