HL incident on 2012-06-20 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,500
Incident datetime
2012-06-20 10:30
Report number
Location
TX
Narrative
A enterprise pipeline technician got a call from the control center that they had received two calls about crude oil spraying out on the ground near the mainline pump discharge piping at lagrange station. The control center was asked to shutdown the pump until someone could check it out. The pipeline technician found a back pressure valve on the discharge line of the pump leaking crude oil on the ground. It was estimated about a barrel of crude oil had leaked out before the pump could be shutdown. Clean up crews was called out to remove the contaminated soil. Maintenance crews repaired the back pressure valve.
Detailed record list
Report Received Date
2012-07-06 00:00:00
Iyear
2012
Report Number
20120208
Supplemental Number
17523
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-06-20 10:27:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Intentional Release Bbls
0
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-06-20 10:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-06-20 11:05:00
Restart Datetime
2012-06-20 16:00:00
On Site Datetime
2012-06-20 11:05:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
La Grange Station
Segment Name
C8
Onshore State Abbreviation
Tx
Onshore Postal Code
78945
Onshore City Name
La Grange
Onshore County Name
Fayette
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Relief Valve
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
2500
Est Cost Emergency
0
Est Cost Environmental
2856
Est Cost Other
0
Prpty
5456
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Preparer Name
C********** H****
Prepared Date
2013-03-14 00:00:00
Authorizer Name
C********** H****
Authorizer Telephone
713-381-6304
Authorizer Email
C******@e****.com
Narrative
A enterprise pipeline technician got a call from the control center that they had received two calls about crude oil spraying out on the ground near the mainline pump discharge piping at lagrange station. The control center was asked to shutdown the pump until someone could check it out. The pipeline technician found a back pressure valve on the discharge line of the pump leaking crude oil on the ground. It was estimated about a barrel of crude oil had leaked out before the pump could be shutdown. Clean up crews was called out to remove the contaminated soil. Maintenance crews repaired the back pressure valve.
Report Received Date 2012-07-06 00:00:00
Iyear 2012
Report Number 20120208
Supplemental Number 17523
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2012-06-20 10:27:00
Location Latitude 29.952222 Google Maps OpenStreetMap
Location Longitude -96.861139 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Intentional Release Bbls 0
Recovered Bbls 0.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2012-06-20 10:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-06-20 11:05:00
Restart Datetime 2012-06-20 16:00:00
On Site Datetime 2012-06-20 11:05:00
Ignite Ind No
Explode Ind No
Pipe Fac Name La Grange Station
Segment Name C8
Onshore State Abbreviation Tx
Onshore Postal Code 78945
Onshore City Name La Grange
Onshore County Name Fayette
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Relief Valve
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 2500
Est Cost Emergency 0
Est Cost Environmental 2856
Est Cost Other 0
Prpty 5456
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Preparer Name C********** H****
Prepared Date 2013-03-14 00:00:00
Authorizer Name C********** H****
Authorizer Telephone 713-381-6304
Authorizer Email C******@e****.com
Narrative A enterprise pipeline technician got a call from the control center that they had received two calls about crude oil spraying out on the ground near the mainline pump discharge piping at lagrange station. The control center was asked to shutdown the pump until someone could check it out. The pipeline technician found a back pressure valve on the discharge line of the pump leaking crude oil on the ground. It was estimated about a barrel of crude oil had leaked out before the pump could be shutdown. Clean up crews was called out to remove the contaminated soil. Maintenance crews repaired the back pressure valve.

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