HL incident on 2012-06-05 — PA

Operator
Buckeye Partners, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000,000
Incident datetime
2012-06-05 10:30
Report number
Location
PA
Narrative
At 10:30 am on june 5, 2012, a local operations employee noticed a stain on the side of tank 508 at the mantua station. Emergency response procedures were initiated and the tank was isolated. All appropriate notifications were made. No product impacted the ground. The tank has been emptied and an inspection of the floor was completed on june 28, 2012. It appears that there is a small hole in the tank sump. A repair and remediation plan is being developed. At the time of this submission, the costs have not yet reached the $50,000 reporting threshold, but they are expected to exceed it eventually. The investigation is ongoing. A supplemental report will be filed when more information becomes available. Update root cause a hole in the sump weld allowed product to seep into the sand and gravel between the original bottom and second bottom of the tank. Product was able to escape through the void that existed between the second bottom chime and dead shell that lacked a caulk seal and was never seal welded. Other details the tank bottom is being replaced. Repairs are expected to be completed in june of 2013
Detailed record list
Report Received Date
2012-06-29 00:00:00
Iyear
2012
Report Number
20120201
Supplemental Number
18303
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
Five Tek Park
Operator City Name
Breinigsville
Operator State Abbreviation
PA
Operator Postal Code
18031
Local Datetime
2012-06-05 10:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
0.02
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2012-06-05 10:30:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
On Site Datetime
2012-06-05 10:30:00
Nrc Rpt Datetime
2012-06-05 16:30:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Mantua Station
Segment Name
Ge
Onshore State Abbreviation
Oh
Onshore Postal Code
44255
Onshore City Name
Mantua
Onshore County Name
Portage
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Double Bottom System
Tank Type
Atmospheric
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
1000000
Est Cost Emergency
495000
Est Cost Environmental
28241
Est Cost Other
0
Prpty
1523241
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Additional Installation Ind
Yes
Preparer Name
H*** S******
Preparer Title
Sr Compliance Specialist
Preparer Email
H*******@b******.com
Preparer Telephone
610-904-4916
Prepared Date
2013-07-19 00:00:00
Authorizer Name
J*** R*******
Authorizer Telephone
610-904-4185
Authorizer Title
Compliance Manager
Authorizer Email
J********@b******.com
Narrative
At 10:30 am on june 5, 2012, a local operations employee noticed a stain on the side of tank 508 at the mantua station. Emergency response procedures were initiated and the tank was isolated. All appropriate notifications were made. No product impacted the ground. The tank has been emptied and an inspection of the floor was completed on june 28, 2012. It appears that there is a small hole in the tank sump. A repair and remediation plan is being developed. At the time of this submission, the costs have not yet reached the $50,000 reporting threshold, but they are expected to exceed it eventually. The investigation is ongoing. A supplemental report will be filed when more information becomes available. Update root cause a hole in the sump weld allowed product to seep into the sand and gravel between the original bottom and second bottom of the tank. Product was able to escape through the void that existed between the second bottom chime and dead shell that lacked a caulk seal and was never seal welded. Other details the tank bottom is being replaced. Repairs are expected to be completed in june of 2013
Report Received Date 2012-06-29 00:00:00
Iyear 2012
Report Number 20120201
Supplemental Number 18303
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address Five Tek Park
Operator City Name Breinigsville
Operator State Abbreviation PA
Operator Postal Code 18031
Local Datetime 2012-06-05 10:30:00
Location Latitude 41.286642 Google Maps OpenStreetMap
Location Longitude -81.211906 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 0.02
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2012-06-05 10:30:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
On Site Datetime 2012-06-05 10:30:00
Nrc Rpt Datetime 2012-06-05 16:30:00
Nrc Rpt Num 1013637 NRC Report How to search
Ignite Ind No
Explode Ind No
Pipe Fac Name Mantua Station
Segment Name Ge
Onshore State Abbreviation Oh
Onshore Postal Code 44255
Onshore City Name Mantua
Onshore County Name Portage
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Double Bottom System
Tank Type Atmospheric
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 1000000
Est Cost Emergency 495000
Est Cost Environmental 28241
Est Cost Other 0
Prpty 1523241
Accident Psig 0
Mop Psig 0
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Additional Installation Ind Yes
Preparer Name H*** S******
Preparer Title Sr Compliance Specialist
Preparer Email H*******@b******.com
Preparer Telephone 610-904-4916
Prepared Date 2013-07-19 00:00:00
Authorizer Name J*** R*******
Authorizer Telephone 610-904-4185
Authorizer Title Compliance Manager
Authorizer Email J********@b******.com
Narrative At 10:30 am on june 5, 2012, a local operations employee noticed a stain on the side of tank 508 at the mantua station. Emergency response procedures were initiated and the tank was isolated. All appropriate notifications were made. No product impacted the ground. The tank has been emptied and an inspection of the floor was completed on june 28, 2012. It appears that there is a small hole in the tank sump. A repair and remediation plan is being developed. At the time of this submission, the costs have not yet reached the $50,000 reporting threshold, but they are expected to exceed it eventually. The investigation is ongoing. A supplemental report will be filed when more information becomes available. Update root cause a hole in the sump weld allowed product to seep into the sand and gravel between the original bottom and second bottom of the tank. Product was able to escape through the void that existed between the second bottom chime and dead shell that lacked a caulk seal and was never seal welded. Other details the tank bottom is being replaced. Repairs are expected to be completed in june of 2013

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