HL incident on 2012-05-18 — TX

Operator
Sunoco Pipeline L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,350
Incident datetime
2012-05-18 20:00
Report number
Location
TX
Narrative
Internal corrosion on a dead leg section of 16" tank fill line piping. Dead leg piping has been removed. Re-submitted on 3/20/2013 to include part e5f per PHMSA request.
Detailed record list
Report Received Date
2012-06-14 00:00:00
Iyear
2012
Report Number
20120184
Supplemental Number
17627
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-05-18 20:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
10
Intentional Release Bbls
0
Recovered Bbls
8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2012-05-18 20:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Segment Was Down At The Time Of Discovery.
On Site Datetime
2012-05-18 20:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Corsicana Station
Segment Name
16" Tank Fill Line
Onshore State Abbreviation
Tx
Onshore Postal Code
75110
Onshore City Name
Corsicana
Onshore County Name
Navarro
Designated Location
Survey Station No.
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
12
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
16
Pipe Wall Thickness
0.25
Pipe Smys
42000
Pipe Specification
X42
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
None
Manufactured Year
1953
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
176
Est Cost Prop Damage
1350
Est Cost Emergency
783
Est Cost Environmental
8145
Est Cost Other
0
Prpty
10454
Accident Psig
60
Mop Psig
125
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Small amount would not be detectable by scada
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
K****** D**** B***
Preparer Title
Area Dot Compliance Supervisor
Preparer Email
K*****@s**************.com
Preparer Telephone
281-637-6497
Preparer Fax
281-637-6425
Prepared Date
2013-03-20 00:00:00
Authorizer Name
K****** D**** B***
Authorizer Telephone
281-637-6497
Authorizer Title
Area Dot Compliance Supervisor
Authorizer Email
K*****@s**************.com
Narrative
Internal corrosion on a dead leg section of 16" tank fill line piping. Dead leg piping has been removed. Re-submitted on 3/20/2013 to include part e5f per PHMSA request.
Report Received Date 2012-06-14 00:00:00
Iyear 2012
Report Number 20120184
Supplemental Number 17627
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2012-05-18 20:00:00
Location Latitude 32.0729 Google Maps OpenStreetMap
Location Longitude -96.4767 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 10
Intentional Release Bbls 0
Recovered Bbls 8
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2012-05-18 20:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Segment Was Down At The Time Of Discovery.
On Site Datetime 2012-05-18 20:30:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Corsicana Station
Segment Name 16" Tank Fill Line
Onshore State Abbreviation Tx
Onshore Postal Code 75110
Onshore City Name Corsicana
Onshore County Name Navarro
Designated Location Survey Station No.
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 12
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 16
Pipe Wall Thickness 0.25
Pipe Smys 42000
Pipe Specification X42
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type None
Manufactured Year 1953
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 176
Est Cost Prop Damage 1350
Est Cost Emergency 783
Est Cost Environmental 8145
Est Cost Other 0
Prpty 10454
Accident Psig 60
Mop Psig 125
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Small amount would not be detectable by scada
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Preparer Name K****** D**** B***
Preparer Title Area Dot Compliance Supervisor
Preparer Email K*****@s**************.com
Preparer Telephone 281-637-6497
Preparer Fax 281-637-6425
Prepared Date 2013-03-20 00:00:00
Authorizer Name K****** D**** B***
Authorizer Telephone 281-637-6497
Authorizer Title Area Dot Compliance Supervisor
Authorizer Email K*****@s**************.com
Narrative Internal corrosion on a dead leg section of 16" tank fill line piping. Dead leg piping has been removed. Re-submitted on 3/20/2013 to include part e5f per PHMSA request.

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