HL incident on 2012-05-14 — OK

Operator
Magellan Terminals Holdings, Lp
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2012-05-14 07:00
Report number
Location
OK
Narrative
At 0700 on 5/14/12, an operator discovered oil on a containment pond that came throught the external floating roof drain. The roof drain valve was closed to isolate the leak source and contractors were contacted. After further investigation it was determined that a reinforcing pad around a roof support leg began to leak due to a weld defect. It was later determined that the tank needed to be taken out of service and cleaned to be repaired. Repairs included grinding out the weld and re-welding the repad. They also welded the underside of the repad as well to ensure the repair of the leak. A dye test was performed for verification. The cost exceeded the $50,000 criteria due to the $112,000 to clean the tank and external roof.
Detailed record list
Report Received Date
2012-06-13 00:00:00
Iyear
2012
Report Number
20120181
Supplemental Number
17840
Report Type
Supplemental Final
Operator Id
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2012-05-14 07:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.71
Intentional Release Bbls
0
Recovered Bbls
0.71
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2012-05-14 07:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
On Site Datetime
2012-05-14 07:00:00
Nrc Rpt Datetime
2012-06-12 06:18:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
South Cushing Crude
Segment Name
Tank #2511
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Adair
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Fillet Weld
Tank Type
Atmospheric
Installation Year
2011
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
10000
Est Cost Emergency
3000
Est Cost Environmental
0
Est Cost Other
112000
Est Cost Other Details
Cost Of Cleaning The Tank For Repairs And Cleaning Off External Floating Roof
Prpty
125000
Accident Psig
3
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was a roof drain / reinforcing pad around a supporting roof leg and amount was under the detectable limits for a controller to detect.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Weld Quality
Additional Lack Fusion Ind
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
Yes
Exm Other Type
At Time Of Repair Of The Support Leg Reinforcement Pad A Diesel Test Was Performed For The Top Weld And Then A Dye Penetrant Test Was Performed After The Underside Weld Was Completed.
Exm Other Rcnt Year
2012
Exm Other Rcnt Ind
Yes
Preparer Name
D******* C*********
Preparer Title
Compliance Coordinator Sr
Preparer Email
D******************@m*********.com
Prepared Date
2013-04-08 00:00:00
Authorizer Name
D******* C*********
Authorizer Telephone
9185747386
Authorizer Email
No Email Address
Narrative
At 0700 on 5/14/12, an operator discovered oil on a containment pond that came throught the external floating roof drain. The roof drain valve was closed to isolate the leak source and contractors were contacted. After further investigation it was determined that a reinforcing pad around a roof support leg began to leak due to a weld defect. It was later determined that the tank needed to be taken out of service and cleaned to be repaired. Repairs included grinding out the weld and re-welding the repad. They also welded the underside of the repad as well to ensure the repair of the leak. A dye test was performed for verification. The cost exceeded the $50,000 criteria due to the $112,000 to clean the tank and external roof.
Report Received Date 2012-06-13 00:00:00
Iyear 2012
Report Number 20120181
Supplemental Number 17840
Report Type Supplemental Final
Operator Id 31580 PHMSA Enforcement
Name Magellan Terminals Holdings, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2012-05-14 07:00:00
Location Latitude 35.92536 Google Maps OpenStreetMap
Location Longitude -96.74162 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.71
Intentional Release Bbls 0
Recovered Bbls 0.71
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2012-05-14 07:00:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
On Site Datetime 2012-05-14 07:00:00
Nrc Rpt Datetime 2012-06-12 06:18:00
Nrc Rpt Num 1014367 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name South Cushing Crude
Segment Name Tank #2511
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Adair
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Weld Subtype Fillet Weld
Tank Type Atmospheric
Installation Year 2011
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 10000
Est Cost Emergency 3000
Est Cost Environmental 0
Est Cost Other 112000
Est Cost Other Details Cost Of Cleaning The Tank For Repairs And Cleaning Off External Floating Roof
Prpty 125000
Accident Psig 3
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was a roof drain / reinforcing pad around a supporting roof leg and amount was under the detectable limits for a controller to detect.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details Weld Quality
Additional Lack Fusion Ind Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind Yes
Exm Other Type At Time Of Repair Of The Support Leg Reinforcement Pad A Diesel Test Was Performed For The Top Weld And Then A Dye Penetrant Test Was Performed After The Underside Weld Was Completed.
Exm Other Rcnt Year 2012
Exm Other Rcnt Ind Yes
Preparer Name D******* C*********
Preparer Title Compliance Coordinator Sr
Preparer Email D******************@m*********.com
Prepared Date 2013-04-08 00:00:00
Authorizer Name D******* C*********
Authorizer Telephone 9185747386
Authorizer Email No Email Address
Narrative At 0700 on 5/14/12, an operator discovered oil on a containment pond that came throught the external floating roof drain. The roof drain valve was closed to isolate the leak source and contractors were contacted. After further investigation it was determined that a reinforcing pad around a roof support leg began to leak due to a weld defect. It was later determined that the tank needed to be taken out of service and cleaned to be repaired. Repairs included grinding out the weld and re-welding the repad. They also welded the underside of the repad as well to ensure the repair of the leak. A dye test was performed for verification. The cost exceeded the $50,000 criteria due to the $112,000 to clean the tank and external roof.

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