HL incident on 2012-05-15 — KS

Operator
Koch Pipeline Company, L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$40,221
Incident datetime
2012-05-15 10:57
Report number
Location
KS
Narrative
An in-line pressure relief check valve, for thermal protection of the outgoing launcher trap, was being replaced because it had failed during the annual inspection and test. During the change out of the in-line pressure relief, the relief line discharge 1/2" ball valve connected to the top of the 20" mainline aboveground piping remained in the open position, allowed the release. An operator qualified koch pipeline employee properly isolated the upstream piping to the in-line relief, but failed to close the discharge 1/2" ball valve that would have isolated the downstream piping of the in-line relief. Upstream piping was removed first without issue but during removal of the in-line relief, pipeline pressure from the downstream side was directly against the in-line relief as it was unscrewed, forcing the in-line relief to separate from the tubing causing the release. The amount of soil remediated due to impact was approximately 100.32 tons.
Detailed record list
Report Received Date
2012-06-07 00:00:00
Iyear
2012
Report Number
20120175
Supplemental Number
18893
Report Type
Supplemental Final
Operator Id
Name
Koch Pipeline Company, L.p.
Operator Street Address
4111 East 37th Street North, , Po Box 2913
Operator City Name
Wichita
Operator State Abbreviation
KS
Operator Postal Code
67220
Local Datetime
2012-05-15 10:57:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
3.2
Intentional Release Bbls
0
Recovered Bbls
2.62
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2012-05-15 10:57:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Had Been Shutdown Prior To Release For Scheduling Reasons.
On Site Datetime
2012-05-15 14:00:00
Nrc Rpt Datetime
2012-05-15 11:38:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Jacksonville Station
Segment Name
Index 5042
Onshore State Abbreviation
Mo
Onshore Postal Code
65239
Onshore City Name
Jacksonville
Onshore County Name
Randolph
Designated Location
Milepost/valve Station
Designated Name
141
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Relief Line And Relief Equipment
Installation Year
1993
Material Involved
Material Other Than Carbon Steel
Material Details
1/2" Steel Valve Connected To Ss Tubing
Release Type
Leak
Leak Type
Other
Leak Type Other
1/2" Ball Valve
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
10016
Est Cost Gas Released
300
Est Cost Prop Damage
40221
Est Cost Emergency
0
Est Cost Environmental
46494
Est Cost Other
0
Prpty
97031
Accident Psig
459
Mop Psig
1170
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Local personnel was on site performing maintenance work of the relief valve. The controller was not performing any work that affected personnel's work.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related No Proc Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
C**** K******
Preparer Title
Program Coordinator
Preparer Email
C*************@k***********.com
Preparer Telephone
316-828-4121
Preparer Fax
316-529-6377
Prepared Date
2014-01-03 00:00:00
Authorizer Name
C**** K*******
Authorizer Telephone
316-828-4121
Authorizer Title
Program Coordinator
Authorizer Email
C*************@k***********.com
Narrative
An in-line pressure relief check valve, for thermal protection of the outgoing launcher trap, was being replaced because it had failed during the annual inspection and test. During the change out of the in-line pressure relief, the relief line discharge 1/2" ball valve connected to the top of the 20" mainline aboveground piping remained in the open position, allowed the release. An operator qualified koch pipeline employee properly isolated the upstream piping to the in-line relief, but failed to close the discharge 1/2" ball valve that would have isolated the downstream piping of the in-line relief. Upstream piping was removed first without issue but during removal of the in-line relief, pipeline pressure from the downstream side was directly against the in-line relief as it was unscrewed, forcing the in-line relief to separate from the tubing causing the release. The amount of soil remediated due to impact was approximately 100.32 tons.
Report Received Date 2012-06-07 00:00:00
Iyear 2012
Report Number 20120175
Supplemental Number 18893
Report Type Supplemental Final
Operator Id 22855 PHMSA Enforcement
Name Koch Pipeline Company, L.p.
Operator Street Address 4111 East 37th Street North, , Po Box 2913
Operator City Name Wichita
Operator State Abbreviation KS
Operator Postal Code 67220
Local Datetime 2012-05-15 10:57:00
Location Latitude 39.5894 Google Maps OpenStreetMap
Location Longitude -92.38284 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 3.2
Intentional Release Bbls 0
Recovered Bbls 2.62
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2012-05-15 10:57:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Had Been Shutdown Prior To Release For Scheduling Reasons.
On Site Datetime 2012-05-15 14:00:00
Nrc Rpt Datetime 2012-05-15 11:38:00
Nrc Rpt Num 1011574 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Jacksonville Station
Segment Name Index 5042
Onshore State Abbreviation Mo
Onshore Postal Code 65239
Onshore City Name Jacksonville
Onshore County Name Randolph
Designated Location Milepost/valve Station
Designated Name 141
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Relief Line And Relief Equipment
Installation Year 1993
Material Involved Material Other Than Carbon Steel
Material Details 1/2" Steel Valve Connected To Ss Tubing
Release Type Leak
Leak Type Other
Leak Type Other 1/2" Ball Valve
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 10016
Est Cost Gas Released 300
Est Cost Prop Damage 40221
Est Cost Emergency 0
Est Cost Environmental 46494
Est Cost Other 0
Prpty 97031
Accident Psig 459
Mop Psig 1170
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Local personnel was on site performing maintenance work of the relief valve. The controller was not performing any work that affected personnel's work.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related No Proc Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name C**** K******
Preparer Title Program Coordinator
Preparer Email C*************@k***********.com
Preparer Telephone 316-828-4121
Preparer Fax 316-529-6377
Prepared Date 2014-01-03 00:00:00
Authorizer Name C**** K*******
Authorizer Telephone 316-828-4121
Authorizer Title Program Coordinator
Authorizer Email C*************@k***********.com
Narrative An in-line pressure relief check valve, for thermal protection of the outgoing launcher trap, was being replaced because it had failed during the annual inspection and test. During the change out of the in-line pressure relief, the relief line discharge 1/2" ball valve connected to the top of the 20" mainline aboveground piping remained in the open position, allowed the release. An operator qualified koch pipeline employee properly isolated the upstream piping to the in-line relief, but failed to close the discharge 1/2" ball valve that would have isolated the downstream piping of the in-line relief. Upstream piping was removed first without issue but during removal of the in-line relief, pipeline pressure from the downstream side was directly against the in-line relief as it was unscrewed, forcing the in-line relief to separate from the tubing causing the release. The amount of soil remediated due to impact was approximately 100.32 tons.

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