HL incident on 2012-05-08 — OK

Operator
Explorer Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$16,000
Incident datetime
2012-05-08 07:04
Report number
Location
OK
Narrative
On may 8, 2012 at approximately 07:00 an employee noted that an alternate suction valve at the gerald, missouri pump station was leaking from the top of the yoke tube. The valve involved was closed at the time the leak was identified as well as the pump station was isolated. The employee requested the pipeline shut down at 07:04 and responded to the valve. The source of the leak was a snap ring that had broken and allowed the valve packing to extrude and product into the yoke tube. The valve was repaired and all the impacted soil was tested, excavated and properly managed. Report was supplmented to account for question e5f.
Detailed record list
Report Received Date
2012-06-01 00:00:00
Iyear
2012
Report Number
20120170
Supplemental Number
18357
Report Type
Supplemental Final
Operator Id
Name
Explorer Pipeline Co
Operator Street Address
Po Box 2650
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74101
Local Datetime
2012-05-08 07:04:00
Location Latitude
Location Longitude
-91.32391233
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.71
Intentional Release Bbls
0
Recovered Bbls
0.71
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-05-08 07:04:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-05-08 07:04:00
Restart Datetime
2012-05-08 23:15:00
On Site Datetime
2012-05-08 09:15:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Gerald Pump Station
Segment Name
Gearld Pump Station
Onshore State Abbreviation
Mo
Onshore Postal Code
63037
Onshore City Name
Gerald
Onshore County Name
Franklin
Designated Location
Milepost/valve Station
Designated Name
316.5
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
25
Est Cost Prop Damage
16000
Est Cost Emergency
5000
Est Cost Environmental
3500
Est Cost Other
0
Prpty
24525
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Preparer Name
K**** E* B****
Preparer Title
Dot Administrator
Preparer Email
K*****@e***.com
Preparer Telephone
9184935104
Prepared Date
2013-07-30 00:00:00
Authorizer Name
J** S****
Authorizer Telephone
9184935143
Authorizer Title
Director Hsse
Authorizer Email
J*****@e***.com
Narrative
On may 8, 2012 at approximately 07:00 an employee noted that an alternate suction valve at the gerald, missouri pump station was leaking from the top of the yoke tube. The valve involved was closed at the time the leak was identified as well as the pump station was isolated. The employee requested the pipeline shut down at 07:04 and responded to the valve. The source of the leak was a snap ring that had broken and allowed the valve packing to extrude and product into the yoke tube. The valve was repaired and all the impacted soil was tested, excavated and properly managed. Report was supplmented to account for question e5f.
Report Received Date 2012-06-01 00:00:00
Iyear 2012
Report Number 20120170
Supplemental Number 18357
Report Type Supplemental Final
Operator Id 4805 PHMSA Enforcement
Name Explorer Pipeline Co
Operator Street Address Po Box 2650
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74101
Local Datetime 2012-05-08 07:04:00
Location Latitude 38.35257318 Google Maps OpenStreetMap
Location Longitude -91.32391233 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.71
Intentional Release Bbls 0
Recovered Bbls 0.71
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2012-05-08 07:04:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-05-08 07:04:00
Restart Datetime 2012-05-08 23:15:00
On Site Datetime 2012-05-08 09:15:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Gerald Pump Station
Segment Name Gearld Pump Station
Onshore State Abbreviation Mo
Onshore Postal Code 63037
Onshore City Name Gerald
Onshore County Name Franklin
Designated Location Milepost/valve Station
Designated Name 316.5
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 25
Est Cost Prop Damage 16000
Est Cost Emergency 5000
Est Cost Environmental 3500
Est Cost Other 0
Prpty 24525
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Preparer Name K**** E* B****
Preparer Title Dot Administrator
Preparer Email K*****@e***.com
Preparer Telephone 9184935104
Prepared Date 2013-07-30 00:00:00
Authorizer Name J** S****
Authorizer Telephone 9184935143
Authorizer Title Director Hsse
Authorizer Email J*****@e***.com
Narrative On may 8, 2012 at approximately 07:00 an employee noted that an alternate suction valve at the gerald, missouri pump station was leaking from the top of the yoke tube. The valve involved was closed at the time the leak was identified as well as the pump station was isolated. The employee requested the pipeline shut down at 07:04 and responded to the valve. The source of the leak was a snap ring that had broken and allowed the valve packing to extrude and product into the yoke tube. The valve was repaired and all the impacted soil was tested, excavated and properly managed. Report was supplmented to account for question e5f.

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