Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2012-04-25 — TX
Operator
Enterprise Crude Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$2,000
Incident datetime
2012-04-25 07:00
Report number
Location
TX
Narrative
Enterprise field tech. Found oil on the ground at addington station. It was determined that during a booster replacement and operational valve re-alignment the day before a valve was left closed that provides thermal relief. The psi build up caused the failure of a gasket on a pd meter. 15 gallons released in the station manifold area. All oil contained to the property. Crew repaired the meter and replaced the gravel.
Detailed record list
Report Received Date
2012-05-17 00:00:00
Iyear
2012
Report Number
20120160
Supplemental Number
17450
Report Type
Supplemental Final
Operator Id
30829
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-04-25 06:30:00
Location Latitude
34.244372
Location Longitude
-97.948581
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Intentional Release Bbls
0
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-04-25 07:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
On Site Datetime
2012-04-25 08:00:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Addington Station
Segment Name
C22
Onshore State Abbreviation
Ok
Onshore Postal Code
73520
Onshore City Name
Addington
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Mp 0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
2000
Est Cost Emergency
0
Est Cost Environmental
8000
Est Cost Other
0
Prpty
10050
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Preparer Name
C********** H****
Preparer Email
C******@e****.com
Preparer Telephone
713-381-6304
Prepared Date
2013-03-11 00:00:00
Authorizer Name
C********** H****
Authorizer Telephone
713-381-6304
Authorizer Title
Pipeline Compliance Specialist
Authorizer Email
C******@e****.com
Narrative
Enterprise field tech. Found oil on the ground at addington station. It was determined that during a booster replacement and operational valve re-alignment the day before a valve was left closed that provides thermal relief. The psi build up caused the failure of a gasket on a pd meter. 15 gallons released in the station manifold area. All oil contained to the property. Crew repaired the meter and replaced the gravel.
| Report Received Date | 2012-05-17 00:00:00 |
|---|---|
| Iyear | 2012 |
| Report Number | 20120160 |
| Supplemental Number | 17450 |
| Report Type | Supplemental Final |
| Operator Id | 30829 PHMSA Enforcement |
| Name | Enterprise Crude Pipeline Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2012-04-25 06:30:00 |
| Location Latitude | 34.244372 Google Maps OpenStreetMap |
| Location Longitude | -97.948581 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.5 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0.2 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2012-04-25 07:00:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| On Site Datetime | 2012-04-25 08:00:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | Addington Station |
| Segment Name | C22 |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 73520 |
| Onshore City Name | Addington |
| Onshore County Name | Jefferson |
| Designated Location | Milepost/valve Station |
| Designated Name | Mp 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Meter/prover |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 50 |
| Est Cost Prop Damage | 2000 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 8000 |
| Est Cost Other | 0 |
| Prpty | 10050 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Incorrect Operation |
| Cause Details | Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure |
| Operation Type | Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure |
| Preparer Name | C********** H**** |
| Preparer Email | C******@e****.com |
| Preparer Telephone | 713-381-6304 |
| Prepared Date | 2013-03-11 00:00:00 |
| Authorizer Name | C********** H**** |
| Authorizer Telephone | 713-381-6304 |
| Authorizer Title | Pipeline Compliance Specialist |
| Authorizer Email | C******@e****.com |
| Narrative | Enterprise field tech. Found oil on the ground at addington station. It was determined that during a booster replacement and operational valve re-alignment the day before a valve was left closed that provides thermal relief. The psi build up caused the failure of a gasket on a pd meter. 15 gallons released in the station manifold area. All oil contained to the property. Crew repaired the meter and replaced the gravel. |
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