Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2012-04-11 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$25
Incident datetime
2012-04-11 11:30
Report number
Location
OK
Narrative
During a regularly scheduled mainline block valve inspection, the packing around the valve stem was discovered to be leaking, magellan personnel completed the inspection and replaced the packing material, stopping the leak. Impacted soil was remediated according to company and state standards.
Detailed record list
Report Received Date
2012-05-10 00:00:00
Iyear
2012
Report Number
20120150
Supplemental Number
16857
Report Type
Supplemental Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2012-04-11 11:30:00
Location Latitude
45.05919
Location Longitude
-93.19544
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.24
Intentional Release Bbls
0
Recovered Bbls
0.24
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-04-11 11:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Release Was From A Valve Weeping That Did Not Require Shutting Down The Line.
On Site Datetime
2012-04-11 11:30:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
#2-8" Minneapolis -- Duluth Line
Segment Name
Line Id #6215
Onshore State Abbreviation
Mn
Onshore Postal Code
55112
Onshore City Name
New Brighton
Onshore County Name
Ramsey
Designated Location
Milepost/valve Station
Designated Name
2.68
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
25
Est Cost Prop Damage
25
Est Cost Emergency
0
Est Cost Environmental
2000
Est Cost Other
0
Prpty
2050
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7246
Prepared Date
2012-08-24 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
During a regularly scheduled mainline block valve inspection, the packing around the valve stem was discovered to be leaking, magellan personnel completed the inspection and replaced the packing material, stopping the leak. Impacted soil was remediated according to company and state standards.
| Report Received Date | 2012-05-10 00:00:00 |
|---|---|
| Iyear | 2012 |
| Report Number | 20120150 |
| Supplemental Number | 16857 |
| Report Type | Supplemental Final |
| Operator Id | 22610 PHMSA Enforcement |
| Name | Magellan Pipeline Company, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2012-04-11 11:30:00 |
| Location Latitude | 45.05919 Google Maps OpenStreetMap |
| Location Longitude | -93.19544 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Gasoline (Non-Ethanol) |
| Unintentional Release Bbls | 0.24 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0.24 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2012-04-11 11:30:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Release Was From A Valve Weeping That Did Not Require Shutting Down The Line. |
| On Site Datetime | 2012-04-11 11:30:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | #2-8" Minneapolis -- Duluth Line |
| Segment Name | Line Id #6215 |
| Onshore State Abbreviation | Mn |
| Onshore Postal Code | 55112 |
| Onshore City Name | New Brighton |
| Onshore County Name | Ramsey |
| Designated Location | Milepost/valve Station |
| Designated Name | 2.68 |
| Federal | No |
| Location Type | Pipeline Right-Of-Way |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Valve |
| Valve Type | Mainline |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 25 |
| Est Cost Prop Damage | 25 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 2000 |
| Est Cost Other | 0 |
| Prpty | 2050 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Other Equipment Failure |
| Eq Failure Type | Other Equipment Failure |
| Preparer Name | K****** L* L******* |
| Preparer Title | Sr. Compliance Coordinator |
| Preparer Email | K***********@m*********.com |
| Preparer Telephone | 918-574-7315 |
| Preparer Fax | 918-574-7246 |
| Prepared Date | 2012-08-24 00:00:00 |
| Authorizer Name | K****** L* L******* |
| Authorizer Telephone | 918-574-7315 |
| Authorizer Title | Sr. Compliance Coordinator |
| Authorizer Email | K***********@m*********.com |
| Narrative | During a regularly scheduled mainline block valve inspection, the packing around the valve stem was discovered to be leaking, magellan personnel completed the inspection and replaced the packing material, stopping the leak. Impacted soil was remediated according to company and state standards. |
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